Accident Taylorcraft BC12-D N43085,
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ASN Wikibase Occurrence # 297293
 
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Date:Thursday 16 May 2002
Time:06:25 LT
Type:Silhouette image of generic TAYB model; specific model in this crash may look slightly different    
Taylorcraft BC12-D
Owner/operator:Private
Registration: N43085
MSN: 6744
Total airframe hrs:3871 hours
Engine model:Continental A65
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Gaston, Oregon -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Gaston, OR (OR69)
Destination airport:(OR69)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot took his Taylorcraft BC12-D, which had not been inspected for nearly three years and had been sitting in storage for the previous year, and prepped it for flight. During the prepping procedure he drained the fuel (auto gas) from the aircraft, and flushed the tanks and lines with auto gas. He also cleaned the carburetor and screen, removed and cleaned the spark plugs, flushed out old storage oil in the cylinders and adjusted the timing. A week later he took the plane out of the hangar, drained the gas sumps, checked the oil and started the engine and allowed it to warm up to 100 degrees oil temperature. He then ran the engine up to 2300 RPM, checked the carburetor heat and magnetos and then started his takeoff roll. About 40-50 feet above ground and headed northbound from his 800 foot long turf airstrip the engine abruptly quit. The pilot focused his attention inside the aircraft as he attempted to determine the reason for the loss of engine power. During that time the aircraft collided with a power pole beyond the end of the runway and impacted terrain coming to rest in a ditch. An FAA inspector examined the engine and found foreign material in both the gascolator and the carburetor bowl, and corrosion within the left magneto, but no mechanical malfunction was discovered.

Probable Cause: The pilot's failure to maintain clearance from object(s) while executing a forced landing following a total loss of power for undetermined cause(s). Contributing factors where the pole impacted during the emergency landing and the pilot's diverted attention.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA02LA082
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB SEA02LA082

Revision history:

Date/timeContributorUpdates
14-Oct-2022 16:50 ASN Update Bot Added

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