Fuel exhaustion Accident Cessna TR182 N787PC,
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ASN Wikibase Occurrence # 297357
 
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Date:Sunday 28 April 2002
Time:15:30 LT
Type:Silhouette image of generic C82R model; specific model in this crash may look slightly different    
Cessna TR182
Owner/operator:Air West Flight Center Inc.
Registration: N787PC
MSN: R18200867
Engine model:Lycoming O-540-J3C5D
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Kersey, Colorado -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Hastings Airport, NE (HSI/KHSI)
Destination airport:Longmont, CO (2V2)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot said that he flew direct from Longmont, Colorado to Ankeny, Iowa (533 nautical miles), and put 49.2 gallons of fuel in the airplane. On the return flight, he stopped at Hastings, Nebraska for food and a rest stop. He did not put additional fuel in the airplane during the rest stop. He departed for Longmont, Colorado, and experienced a power failure approximately 2.5 hours later; the pilot performed a forced landing to a highway. During the landing sequence, the pilot "extended the landing gear at the last second," and it failed to fully extend. The front door post bulk head was bent and the bottom of the airplane was badly damaged. The pilot said that the airplane held 92 gallons of fuel (88 gallons usable), but they customarily fueled it to the bottom of the fuel necks, which was approximately 65 gallons usable. A representative of the airplane's manufacturer said that the airplane burned approximately 14 to 15 gallons per hour in cruise flight, with 8 gallons being used for the two takeoffs and climbs to cruise altitude. The pilot also said the wind was strong from the west (maybe 30 knots), for the flight to Ankeny, and the return flight to Longmont.




Probable Cause: The pilot's inadequate planning decision which led to fuel exhaustion and subsequent loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN02LA040
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB DEN02LA040

Revision history:

Date/timeContributorUpdates
14-Oct-2022 17:38 ASN Update Bot Added

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