ASN Wikibase Occurrence # 297368
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Date: | Wednesday 24 April 2002 |
Time: | 09:09 LT |
Type: | Cessna 172RG |
Owner/operator: | Holloman Afb Aero Club |
Registration: | N6288R |
MSN: | 172RG0148 |
Year of manufacture: | 1979 |
Total airframe hrs: | 7072 hours |
Engine model: | Lycoming O-360-F1A6 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Alamogordo, New Mexico -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Alamogordo-Holloman AFB, NM (HMN/KHMN) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the CFI and the private pilot no anomalies were noted during the pre-takeoff engine run-up. The air traffic control tower cleared the flight to takeoff from runway 07, at the runway 16 intersection. The private pilot initiated the takeoff roll with the flaps retracted and full fuel. According to a weather observation facility at the air base, at the time of the accident, the wind was from 340 degrees at 11 knots. The manifold pressure, rpm, and engine gauges were all within the set limits during the takeoff roll, and the airplane became airborne. However, once airborne the airplane did not gain airspeed. The pilots maneuvered the airplane into the wind and elected not to retract the landing gear. The CFI stated that he "sensed a lack of adequate power development." The private pilot ensured that the throttle was full forward, reduced the airplane's pitch attitude, and the "airspeed came back weakly;" however, when he increased the pitch attitude, the airspeed "immediately started falling away." The CFI tried a few different mixture settings; however, none increased the power output. The airplane was descending when the private pilot relinquished control of the airplane to the CFI. During the ensuing forced landing, the CFI maneuvered the airplane around a concrete block and landed it in a rough field. The airplane contacted a fence during the roll-out and came to a stop up-right. Post accident examination and test run of the engine did not reveal any anomalies.
Probable Cause: the loss of engine power for an undetermined reason, which resulted in a forced landing after takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW02LA128 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB FTW02LA128
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 17:44 |
ASN Update Bot |
Added |
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