ASN Wikibase Occurrence # 297460
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Date: | Saturday 30 March 2002 |
Time: | 15:15 LT |
Type: | Cessna 210 |
Owner/operator: | Private |
Registration: | N1844F |
MSN: | 21058744 |
Year of manufacture: | 1966 |
Total airframe hrs: | 2999 hours |
Engine model: | Continental IO-520-A29B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Naples, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Naples Airport, FL (APF/KAPF) |
Destination airport: | Tampa-Peter O. Knight Airport, FL (TPF/KTPF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, after departing Naples Airport, he was given clearance to climb to his requested altitude. The pilot reported that, at 800 feet the engine started to lose manifold pressure. Efforts by the pilot to restore manifold pressure were unsuccessful. The pilot declared an emergency and headed back to the Naples airport. When he saw that he would not make the airport; he elected to make an emergency landing in a mangrove swamp 1/4 mile from the airport. The airplane collided with several trees, and came to rest in about three inches of water. Following the airplane's recovery from the swamp, an examination of the cabin found the throttle and mixture controls in their takeoff positions. Examination of the engine compartment found the mixture cable attachment and the fuel control disconnected. The fuel control arm was not deformed from impact. The mixture cable attachment rod-end was not deformed from impact, and the mixture attachment bolt, nut and washer were missing. At the time of this examination, the mixture arm on the fuel control was in the closed or cutoff position. Examination of the airplane's log books found that the fuel control bracket was replaced during a maintenance visit on December 6, 2001. The airframe had accumulated 27.8 hours since that maintenance had been performed.
Probable Cause: Total loss of engine power due to improper maintenance by company maintenance personnel which allowed the mixture control linkage to disconnect in flight which resulted in an emergency descent to landing into unsuitable terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL02LA070 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB ATL02LA070
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 18:50 |
ASN Update Bot |
Added |
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