ASN Wikibase Occurrence # 298170
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Date: | Monday 5 June 2017 |
Time: | 17:00 LT |
Type: | Cessna 172 |
Owner/operator: | |
Registration: | N35700 |
MSN: | 17256916 |
Year of manufacture: | 1968 |
Total airframe hrs: | 3874 hours |
Engine model: | Lycoming Engines IO-360-A1B6 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Chugiak, Alaska -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | ANCHORAGE, AK (AA06) |
Destination airport: | ANCHORAGE, AK (AA06) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, about 1 hour after takeoff on the personal flight, the engine started "sputtering" and then lost all power. The pilot was unable to restart the engine and maneuvered the airplane for landing at a nearby airport. The airplane subsequently touched down in an open field, impacted a fence, and came to rest inverted in the grass, resulting in substantial damage.
During recovery of the airplane, about 1 gallon of fuel was drained from the left wing and about 7.5 gallons of fuel were drained from the right wing. Examination revealed no preimpact mechanical malfunctions or failures with the airframe or engine. The engine was satisfactorily test run several times during the examination. The fuel injector servo successfully passed a flow check and showed no preimpact mechanical malfunctions or failures. Various fuel samples from the airplane were tested and no water was detected.
The pilot initially reported that the fuel selector valve was positioned at the left tank position when the engine started experiencing issues, but later reported that he was using the right tank position during the engine issues. Given the airplane's fuel state following the accident and the lack of anomalies found during postaccident examination, it is likely that the loss of engine power was the result of fuel starvation when the pilot exhausted the fuel supply of the left wing tank.
Probable Cause: The pilot's improper in-flight fuel management, which resulted in a total loss of engine power due to fuel starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC17LA028 |
Status: | Investigation completed |
Duration: | 3 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB ANC17LA028
Location
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 14:03 |
ASN Update Bot |
Added |
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