ASN Wikibase Occurrence # 298203
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Date: | Wednesday 19 December 2001 |
Time: | 20:50 LT |
Type: | Cessna T210N |
Owner/operator: | Gerald Blank |
Registration: | N7AL |
MSN: | 21063261 |
Total airframe hrs: | 1929 hours |
Engine model: | Continental TSIO-520-R |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Diego, California -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | San Diego-Montgomery-Gibbs Executive Airport, CA (MYF/KMYF) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane landed long and continued off the end of the runway into a chain link fence. Nighttime darkness prevailed and the airport weather, observed 3 minutes after the accident, was visibility 1/4 statute mile, vertical visibility 100 feet, with temperature and dew point both 9 degrees Celsius. A sheriff's deputy reported from the accident site that the visibility was 50 to 100 yards in fog. The pilot reported that the accident occurred as he was returning to the departure airport following a 40-minute post maintenance checkflight. He received the airport weather from the Automatic Terminal Information Service (ATIS) recording and was aware that ground fog had developed at the airport. He received air traffic clearance and executed the instrument landing system (ILS) approach. At decision height he was still in visual meteorological conditions and the runway and approach lighting were in sight. The pilot continued his descent below decision height by visual reference and encountered dense fog and severe restriction to visibility at 50 to 75 feet above ground level. The pilot did not feel a go-around was possible at that point and continued the landing approach, landing long on the runway and continuing off the end.
Probable Cause: The pilot's failure to land on the runway with sufficient runway remaining as a result of his improper IFR procedure by his failure to maintain visual contact with the runway environment, and to execute a missed approach.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX02LA053 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB LAX02LA053
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 15:13 |
ASN Update Bot |
Added |
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