ASN Wikibase Occurrence # 298469
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Date: | Saturday 22 September 2001 |
Time: | 18:40 LT |
Type: | Boeing-Stearman B75N1 |
Owner/operator: | Richard Thomas Parrish |
Registration: | N47964 |
MSN: | 75-7540 |
Total airframe hrs: | 3258 hours |
Engine model: | Continental W670 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Carbondale, Illinois -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Shelbyville, IL (2H0) |
Destination airport: | Carbondale-Southern Illinois Airport, IL (MDH/KMDH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was attempting a night landing on a sod area to the right side of the runway and landed approximately 150 feet to the right of the sod area in a cornfield. The pilot reported, "Because of ditch to left and low light conditions approach was to right of center of sod. Approach was 35 yards too far to right and when ground was in sight for landing, the tassels of a cornfield were mistaken for grass runway. A normal 3 point full stall landing was made to the tops of corn, proceeding for 100 feet and a very slow pitch over onto nose and back." According to an almanac of sun data, the sun set at 1854 and the end of civil twilight was at 1920. The Southern Illinois Airport Authority (SIAA) approved takeoff and landing operations on the sod area adjacent to runway 36R for two specific pilot/aircraft combinations. The memorandum did not have any additional limitations or provisions, including the restriction of operations after civil twilight. Subsequent to the accident, the SIAA mandated that all flight operations on the sod area would be during daylight hours only.
Probable Cause: The pilot misjudged the proper alignment with the landing area. Contributing to the accident was the light conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI01LA321 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB CHI01LA321
History of this aircraft
Other occurrences involving this aircraft
18 August 2012 |
N47964 |
American Airpower Heritage Flying Museum |
0 |
Mesa, Arizona |
|
sub |
Runway excursion |
19 March 2013 |
N47964 |
Arizona Wing Commemorative Air Force |
0 |
Mesa, Arizona |
|
sub |
Runway excursion |
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 18:22 |
ASN Update Bot |
Added |
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