ASN Wikibase Occurrence # 298507
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Date: | Tuesday 4 September 2001 |
Time: | 19:30 LT |
Type: | Cessna 150J |
Owner/operator: | Craig Aure |
Registration: | N51256 |
MSN: | 15069875 |
Year of manufacture: | 1968 |
Total airframe hrs: | 5070 hours |
Engine model: | Continental O-200A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sonoma, California -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | San Andreas-Calaveras Co Maury Rasmussen Field, CA (KCPU) |
Destination airport: | Sonoma, CA (0Q9) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During an approach for landing the engine lost power and the pilot made a forced landing in a vineyard where the airplane came to rest on it's nose. Fuel was observed in the fuel tanks. Fuel recovered from the fuel tanks was 4.5 gallons. According to the manufacturer, 3.5 gallons of fuel is unusable. During the engine inspection it was noted that the ignition switch was defective and did not allow for proper contact with the system. Pressure had to be applied to the instrument panel in order to allow a positive ground to the system for start up. The pilot indicated that the ignition switch had been defective prior to the accident flight and had been that way for some time. A successful engine ground run was conducted with no further mechanical discrepancies noted. Review of the Carburetor Icing Probability Chart revealed that weather conditions were conducive to serious icing at climb or cruise power.
Probable Cause: Fuel exhaustion due to the pilot's inadequate preflight fuel consumption calculations and failure to ensure that adequate fuel was onboard the airplane prior to departure. A factor in the accident was the pilot's continued use of the airplane with known mechanical deficiencies.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX01LA289 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX01LA289
History of this aircraft
Other occurrences involving this aircraft
8 January 2005 |
N51256 |
Private |
1 |
Marana, AZ |
|
sub |
Collision with pole or wires |
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 18:52 |
ASN Update Bot |
Added |
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