ASN Wikibase Occurrence # 298714
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Date: | Monday 10 July 2000 |
Time: | 09:30 LT |
Type: | Cessna 172L |
Owner/operator: | Private |
Registration: | N3875Q |
MSN: | 17259975 |
Year of manufacture: | 1971 |
Total airframe hrs: | 3256 hours |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | BEAUFORT, North Carolina -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | (KMRH) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight was a maintenance test flight following engine overhaul due to a propeller strike on March 10, 2000. No discrepancies were noted by the pilot during the engine run-up or after applying full power to takeoff. While climbing about 100 feet above ground level (agl), the engine experienced a loss of power then quit. The pilot landed the airplane with only 180 feet remaining on the departure runway and applied heavy brakes. The airplane departed the end of the runway, rolled onto wet grass, and unable to stop the airplane, collided with a chain link fence. The engine was disassembled with FAA approval by the facility that overhauled it without government oversight, before NTSB notification. The No. 4 cylinder connecting rod bolts were fractured, and the connecting rod cap was straight. Due to the lack of government oversight during the examination of the failed engine, no components of the engine were examined or retained. An entry in the maintenance records dated July 5, 2000, indicates that the engine was overhauled '...per Lycoming Overhaul Manual (60294-7).' The entry also indicates that the engine was test run, and 'All pressures and temps [sic] within manufacturer specifications....'
Probable Cause: A loss of engine power due to failure of the No. 4 cylinder connecting rod during the first flight following engine overhaul for undetermined reasons. Contributing to the accident was unsuitable terrain.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | MIA00LA215 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB MIA00LA215
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 21:49 |
ASN Update Bot |
Added |
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