ASN Wikibase Occurrence # 299204
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Date: | Friday 24 March 2000 |
Time: | 16:00 LT |
Type: | Cessna 172 |
Owner/operator: | Obrien Aviation Inc. |
Registration: | N52633 |
MSN: | 17274572 |
Year of manufacture: | 1981 |
Total airframe hrs: | 4290 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | FARMINGDALE, New Jersey -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | , NJ (KBLM) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After the pilot taxied onto the runway for departure, he set the elevator trim wheel 1/2 inch nose down, announced his departure, and applied full power. He reported that he 'felt nose-down pressure from the beginning of the takeoff roll.' As the airplane accelerated, the pilot 'wound off the trim' and at 55 knots, the airplane rotated. The pilot stated that immediately after takeoff, the airplane dove toward the runway. It struck the runway and bounced twice. The airplane then experienced a 'small bounce', and landed on the main gear. The pilot stated that he experienced no flight control difficulties prior to the accident, and reported that the accident could have been caused by many possibilities, including, '...a stall, excessive nose-down trim, or a relaxed yoke.' Additionally, the pilot stated his normal procedure for takeoff was to apply about 1/2 inch of nose-down trim, to 'keep the airplane on the runway.' After the accident, the elevator trim wheel was rotated without restriction, and examination of the airplane revealed no pre-impact failure of the flight controls.
Probable Cause: The pilot's failure to maintain control of the airplane which resulted in an inadvertent stall. A factor in the accident was the pilot's use of excessive nose-down elevator trim.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC00LA102 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB NYC00LA102
Revision history:
Date/time | Contributor | Updates |
16-Oct-2022 03:47 |
ASN Update Bot |
Added |
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