Accident Dornier 328-100 N329MX,
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Date:Monday 20 March 2000
Time:07:31 LT
Type:Silhouette image of generic D328 model; specific model in this crash may look slightly different    
Dornier 328-100
Owner/operator:Air Wisconsin
Registration: N329MX
MSN: 3049
Year of manufacture:1996
Total airframe hrs:7596 hours
Engine model:P&W PW119C
Fatalities:Fatalities: 0 / Occupants: 24
Aircraft damage: Substantial
Category:Accident
Location:Denver International Airport, CO (DEN/KDEN) -   United States of America
Phase: Unknown
Nature:Passenger - Scheduled
Departure airport:BISMARCK , ND (KBIS)
Destination airport:Denver International Airport, CO (DEN/KDEN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During the approach, the flight crew confirmed the landing gear was down and locked. The first officer landed the airplane on runway 35L in a slight left crosswind. When the airplane touched down, the landing gear warning horn sounded. The right main and nose landing gears retracted, and the airplane slid to a halt on the right side of the runway. According to the flight data recorder, the landing gear was extended and indicated down and locked (source data is the position of the nose landing gear). The nose landing gear became "unlocked" (i.e., unsafe) 2 seconds after the radio altitude reached 0 feet. Hydraulic pressure dropped to approximately 2,700 psi momentarily, then returned to normal (about 3,000 psi). The following items were subjected to various tests and no anomalies were noted: proximity switch electronics unit (PSEU), right main landing gear harness and proximity switches, landing gear selector valve, hydraulic pressure sensing valve, landing gear control assembly. Hydraulic fluid samples drawn from the filter pack, right main landing gear down lock assist actuator, and the return line for the landing gear selector valve were analyzed. No significant anomalies were noted. Partial systemic wiring tests were unremarkable.

Probable Cause: uncommanded retraction of the nose and right main landing gears during landing roll for reasons undetermined.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN00FA063
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report

Sources:

NTSB DEN00FA063

Revision history:

Date/timeContributorUpdates
16-Oct-2022 03:58 ASN Update Bot Added

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