ASN Wikibase Occurrence # 30016
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Date: | Tuesday 26 September 2000 |
Time: | 19:00 |
Type: | Beechcraft 55 Baron |
Owner/operator: | Private |
Registration: | N9713R |
MSN: | TC-17 |
Total airframe hrs: | 2770 hours |
Engine model: | Continental IO-470L |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gulfport–Biloxi Airport, Mississippi, -
United States of America
|
Phase: | Approach |
Nature: | Training |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight had completed an ILS approach to runway 36, with a simulated engine out, but did not touch down. The airplane was on final approach when both engines lost power. The CFI said as we turned onto left downwind for runway 36, '...I set zero thrust with the [left] throttle and prop control. About mid field the right engine began to lose power. I turned on both boost pumps and pushed both props and throttles forward. The left engine surged a couple of times but could not produce power. The right engine did not respond...we turned towards the airport...I switched to aux on the fuel tanks and tried to restart to no avail...switched back to mains to no avail. At this time we were about 400 feet agl and realized we would not make the airport. We turned north to land on highway 49...shortly after touchdown the right wing tip hit a light post. We spun around and came to a stop....' Inspection of the wreckage revealed sufficient fuel. Investigators verified flight control continuity, continuity of the fuel system in all positions, the boost pumps worked, and the vents were clear. Both engines were removed from the airplane to facility test runs of the engines, both engines ran, and no discrepancies were found.
Probable Cause: a loss of power on both engines, during a simulated engine out approach, resulting in a forced landing and the subsequent on ground impact with a pole.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA00LA272 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X22041&key=1 FAA register: 1.
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?nNumberTxt=9713R Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
01-Jun-2014 02:25 |
Dr. John Smith |
Updated [Operator, Total fatalities, Total occupants, Other fatalities, Location, Country, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
12-Dec-2017 19:10 |
ASN Update Bot |
Updated [Nature, Departure airport, Destination airport, Source, Narrative] |
06-Jun-2023 05:57 |
Ron Averes |
Updated [[Nature, Departure airport, Destination airport, Source, Narrative]] |
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