Accident Piper PA-32R-300 Cherokee Lance N349SB,
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ASN Wikibase Occurrence # 300325
 
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Date:Sunday 30 October 2022
Time:13:58 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-300 Cherokee Lance
Owner/operator:Skybound Aviation, LLC
Registration: N349SB
MSN: 32R-7780480
Year of manufacture:1977
Total airframe hrs:7189 hours
Engine model:Lycoming IO-540-K1G5D
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Evansville, IN -   United States of America
Phase: En route
Nature:Private
Departure airport:Taylorville Municipal Airport, IL (KTAZ)
Destination airport:Gallatin-Music City Executive Airport, TN (KXNX)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was conducting a personal cross-country flight. He performed a preflight inspection, and the takeoff and climb were normal. After flying for about 1 hour 10 minutes, the pilot felt the engine shake and noticed some abnormal indications on the engine monitor. He made some adjustments to the engine controls, and the engine smoothed out and ran normally. A few minutes later, the engine surged momentarily to full power and then returned to its previous power setting. The pilot diverted to a local airport, and the engine operated normally as the airplane descended. During the approach, which was conducted in instrument meteorological conditions (IMC), the engine lost total power when the airplane was about 8 miles from the airport. The pilot attempted to restart the engine but was unsuccessful. The airplane exited the IMC and subsequently landed hard on a golf course, which resulted in substantial damage to the fuselage, both wings, and horizontal stabilizer.
Postaccident examination of the airplane and extracted engine data revealed no evidence of mechanical malfunctions or failures with the airplane or engine. Given the available evidence for this accident investigation, the reason for the total loss of engine power could not be determined.

Probable Cause: The total loss of engine power for reasons that could not be determined based on the available evidence.

Accident investigation:
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Investigating agency: NTSB
Report number: CEN23LA022
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB CEN23LA022
https://flightaware.com/live/flight/N349SB/history/20221030/1715Z/KTAZ/KXNX

Location

Media:

Revision history:

Date/timeContributorUpdates
30-Oct-2022 20:33 harro Added
30-Oct-2022 20:38 harro Updated [Time, Phase, Departure airport, Destination airport, Source, Embed code, Narrative, Category]
30-Oct-2022 20:42 harro Updated [Destination airport, Embed code]
30-Oct-2022 23:47 RobertMB Updated [Time, Total occupants, Source, Narrative]
01-Nov-2022 08:04 Captain Adam Updated [Narrative]
01-Nov-2022 11:01 Anon. Updated [Narrative]
17-Nov-2022 20:52 Captain Adam Updated [Time, Nature, Destination airport, Source, Embed code, Narrative]
01-Jul-2023 07:21 ASN Update Bot Updated [[Time, Nature, Destination airport, Source, Embed code, Narrative]]
25-Jan-2024 15:07 FxllenCode Updated [Operator, Source, Embed code, Narrative]

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