ASN Wikibase Occurrence # 301078
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 1 February 1998 |
Time: | 17:15 LT |
Type: | Cessna 182 |
Owner/operator: | Private |
Registration: | N7275E |
MSN: | 52275 |
Year of manufacture: | 1959 |
Total airframe hrs: | 5140 hours |
Engine model: | Continental O-470-R |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | EAST MORICHES, New York -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | (1N2) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After three uneventful parachute drop flights with three or four jumpers each, the pilot landed and picked up two jumpers. During the next takeoff roll, the pilot aborted the takeoff and was unable to stop the airplane before it struck a fence at the end of the 2,200 foot asphalt runway. The pilot stated 'everything was normal, except the plane didn't lift off.' He also stated, the airplane was trimmed to 'lift up on it's own' at about 65 MPH, and he aborted the takeoff at about 65 MPH. The pilot used the same elevator trim setting for every takeoff, regardless of how many jumpers were in the airplane. Examination of the airplane did not reveal any mechanical malfunctions of the airframe or engine. The airplane's elevator trim was found in a neutral position. A weight and balance calculation was performed for the accident flight and for a departure with four jumpers. The center of gravity (CG) for the accident flight was about 21.4 inches forward of where the CG would have been located for a parachute drop flight with four jumpers. The CG for the accident flight was 101 inches; the airplane's certificated CG range was from 95 to 113 inches.
Probable Cause: the pilot's improper planning/decision, and failure to attain rotation the airplane for lift-off, which led to an aborted takeoff and collision with a fence. The proximity of the fence was a related factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC98LA064 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB NYC98LA064
Revision history:
Date/time | Contributor | Updates |
13-Nov-2022 13:30 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation