Accident Piper PA-30 Twin Comanche N7295Y,
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ASN Wikibase Occurrence # 301389
 
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Date:Saturday 19 November 2022
Time:11:10
Type:Silhouette image of generic PA30 model; specific model in this crash may look slightly different    
Piper PA-30 Twin Comanche
Owner/operator:Twinkie LLC
Registration: N7295Y
MSN: 30-335
Year of manufacture:1964
Total airframe hrs:5453 hours
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:near Smith Reynolds Airport (INT/KINT), Winston Salem, NC -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:London-Corbin Airport, KY (LOZ/KLOZ)
Destination airport:Winston-Salem-Smith-Reynolds Airport, NC (INT/KINT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On November 19, 2022, about 1110 eastern standard time, a Piper PA-30, N7295Y, was substantially damaged when it was involved in an accident near Smith Reynolds Airport (INT), Winston-Salem, North Carolina. The commercial pilot and passenger were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

Near the conclusion of the cross-country flight, when the airplane was flying about 2,175 ft pressure altitude and about 4 nautical miles due west of the approach end of runway 4 at the destination airport, the pilot broadcast on the frequency that one engine was not making as much power as the other, but that, “we’re ok.” The controller cleared the pilot to land on runway 4; however, for reasons that were not reported by the pilot, the airplane continued past the extended runway centerline for that runway. The pilot subsequently asked to land on runway 33, which was approved. The airplane continued on an easterly heading past the extended runway 33 centerline, then turned left on northwesterly heading flying parallel to runway 33. While flying east of the airport one witness noted the airplane banking left to about 45° before the wings rolled level and then banked about 10° to the left. The same witness reported that, while flying in a nose-up attitude just above the trees with the landing gear extended, the airplane rolled to an inverted position and descended straight down. The airplane impacted terrain behind a house.

Postaccident examination of the flight controls, propellers, right propeller governor, left engine and its systems, and right engine powertrain, lubrication, exhaust, ignition, and air induction systems revealed no evidence of preimpact failure or malfunction. Neither propeller was feathered at impact. The damage to the left propeller was consistent with the engine developing some power at impact while the lack of damage to the right propeller was consistent with windmilling/rotating and not developing power at impact. Additionally, although it was not determined if there were any missing vortex generators (VG’s) on either wing at the time of the accident, the airplane’s performance was not changed by the installation of the VG’s. Thus, if any were missing at the time of the accident, it likely did not contribute to the accident.

Postaccident operational testing of the right engine’s fuel servo revealed that it passed all four test points and the regulator hysteresis check, but it failed testing of the idle circuit, which should result in decreased fuel flow with movement of the throttle control from wide open to idle. The fuel flow when reducing the throttle to idle was about 2.6 times higher than what it should have been. Disassembly of the right fuel servo revealed internal contamination in the fuel section of the regulator that was determined to be acrylonitrile-butadiene-styrene (ABS), a thermoplastic, though the exact source of the contamination could not be determined. Following reassembly of the regulator with the internal contamination removed, the idle circuit test was repeated multiple times, and the fuel flow was within limits. Although it could not be determined if the excessive fuel flow during the idle circuit test was caused by the internal contamination or a combination of that and misalignment of the regulator section, the additional 0.011-inch clearance of the throttle valve at idle was likely the result of maintenance personnel attempting to remedy the excessive fuel flow when moving the throttle valve to idle. Thus, it is likely that during the descent approaching the airport with both engines operating at a reduced power setting, the excessive fuel flow to the right engine likely resulted in a total loss of engine power.

Although the right engine likely sustained a total loss of engine power due to a malfunction of the fuel servo, it is likely that the pilot either did not, or delayed, feathering the right propeller until the propeller rpm slowed to where the propeller blades engaged on the start locks. In that position, an attempt to feather the propeller would not be possible until the propeller rpm increased above the speed that disengaged the start locks. The increased parasitic drag from the windmilling and unfeathered right propeller likely precluded the possibility of straight and level flight. Towards the end of flight, the airspeed likely reduced below the published Velocity Minimum Control (Vmc) speed, and the airplane rolled to an inverted position. Had the pilot either turned towards runway 4 which was the nearest runway after advising the controller of an engine malfunction, or feathered the right propeller following total loss of right engine power and maintained an airspeed above the published Vmc speed while continuing towards the airport, it is likely that he could have reached the airport and landed uneventfully.

Probable Cause: Contamination and/or misalignment of the regulator section of the right engine’s fuel servo, which resulted in excessive idle fuel flow and a total loss of engine power. Also causal was the pilot's failure to land immediately on the nearest runway at the destination airport, his failure to feather the right propeller following the loss of engine power while approaching the airport, and his failure to maintain airspeed while maneuvering with one engine, which resulted in a loss of control at a low altitude.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA23FA067
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

https://journalnow.com/news/local/accident-and-incident/a-plane-with-two-people-on-board-crashes-in-winston-salem/article_c8d7ad64-6832-11ed-a223-634c0069a42a.html

https://data.ntsb.gov/Docket?ProjectID=106324
https://flightaware.com/live/flight/N7295Y

Location

Images:


Photo: NTSB

Media:

Revision history:

Date/timeContributorUpdates
19-Nov-2022 22:10 Geno Added
19-Nov-2022 22:58 Captain Adam Updated [Registration, Cn, Operator, Total fatalities, Phase, Nature, Departure airport, Destination airport, Source, Embed code, Damage, Narrative, Category]
20-Nov-2022 00:32 Iceman 29 Updated [Embed code]
20-Nov-2022 02:39 johnwg Updated [Time, Departure airport, Source, Embed code, Narrative, Category]
20-Nov-2022 08:23 TB Updated [Location, Source]
20-Nov-2022 09:14 Captain Adam Updated [Location, Embed code]
21-Nov-2022 03:14 Anon. Updated [Time, Location, Embed code, Narrative]
08-Mar-2024 03:48 Captain Adam Updated [Phase, Source, Narrative]
08-Mar-2024 04:03 Captain Adam Updated [Accident report, Photo]

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