ASN Wikibase Occurrence # 302844
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Date: | Monday 19 December 2022 |
Time: | 15:00 |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Private |
Registration: | N8137P |
MSN: | E-2653 |
Year of manufacture: | 1991 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | near Harrison-Boone County Airport (HRO/KHRO), AR -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Kansas City-Charles B. Wheeler Downtown Airport, MO (MKC/KMKC) |
Destination airport: | Harrison-Boone County Airport, AR (HRO/KHRO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Beechcraft A36 Bonanza crashed short of the runway after experiening engine problems on approach to Harrison-Boone County Airport (HRO/KHRO), Harrison, Arkansas. There was a post impact fire.
The occupants escaped without injury.
The pilot reported the airplane was topped off with fuel before the flight. He reported that the flight was normal, and he switched fuel tanks when he reached the initial approach fix for the instrument approach. The pilot then canceled his instrument clearance and continued a visual approach to the airport that was normal until he was on short final when the engine stopped producing power. The pilot stated he made one attempt to restore the engine power, which included switching fuel tanks. Unable to restore engine power, the pilot performed a forced landing to a field about one mile short of the runway. During the forced landing the airplane's fuselage was substantially damaged and a postimpact fire ensued, consuming a majority of the fuselage.
A postaccident examination of the engine revealed the engine had been exposed to the postimpact fire. Valvetrain continuity was established throughout the engine. The magnetos and spark plugs were functionally tested and performed normally. The cylinders were examined with a borescope and showed signs of normal wear. The engine fuel components were examined and appeared clear of debris. The remainder of the airplane's fuel system could not be tested due to the postimpact fire. All of the metal propeller blades had chordwise scratches observed on the cambered side as well as nicks and gouges on the leading edges indicative of the propeller producing some amount of power at impact. The engine examination did not reveal any malfunction or failure that would have precluded normal operation of the engine; therefore, the cause of the reported loss of engine power could not be determined.
Probable Cause: A loss of engine power for reasons that could not be determined.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | CEN23LA066 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
https://www.ky3.com/2022/12/20/arkansas-couple-safe-after-plane-crash-just-outside-boone-county-regional-airport/ https://flightaware.com/live/flight/N8137P https://www.aircraft.com/aircraft/1434131/n8137p-1991-beechcraft-a36-bonanza Location
Media:
Revision history:
Date/time | Contributor | Updates |
04-Apr-2024 09:56 |
ASN |
Updated [Narrative, Accident report] |
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