ASN Wikibase Occurrence # 309952
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Date: | Tuesday 22 August 2017 |
Time: | 09:04 LT |
Type: | Enstrom F-28F |
Owner/operator: | Airwest Aviation Academy LLC |
Registration: | N52PD |
MSN: | 807 |
Year of manufacture: | 1996 |
Total airframe hrs: | 6264 hours |
Engine model: | Lycomng HIO-360-F1AD |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Glendale, Arizona -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | Glendale Municipal Airport, AZ (KGEU) |
Destination airport: | Glendale Municipal Airport, AZ (KGEU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor and student pilot were practicing hovering autorotations when the cockpit filled with smoke. The helicopter had just touched down, so the flight instructor secured the cockpit and both he and the student egressed the helicopter with the engine still running. About 5 minutes later, the engine stopped.
Postincident examination of the helicopter revealed no fire or other related damage. Maintenance personnel reported that the smoke appeared to have originated from the failure of an internal oil seal within the turbocharger-compressor that leaked oil into the turbocharger-compressor's exhaust system. No further examination or repair was accomplished and the turbocharger was replaced.
Further examination revealed damage to the turbocharger-compressor v-clamp assembly that was installed on the exhaust. The strap portion of the v-clamp assembly contained cracks on the outer face that emanated from three of the four spot welds. The edge of the strap portion exhibited evidence of bending deformation on both sides of the assembly. In the deformed areas, the distance between the edge of the retainer and the edge of the strap was smaller when compared to other, non-deformed areas. Further, microscopic examination of the largest crack revealed a fatigue crack emanating from the outer surface of the v-clamp assembly strap. It is likely that the v-clamp assembly bolts were tightened to an extent that caused the deformation in the strap. The damage found to the v-clamp was not related to the source of the smoke.
Probable Cause: An internal failure of the turbo-compressor, which resulted in oil leaking into the turbo-compressor's exhaust.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR17IA198 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB WPR17IA198
Location
Revision history:
Date/time | Contributor | Updates |
01-Apr-2023 13:07 |
ASN Update Bot |
Added |
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