ASN Wikibase Occurrence # 311356
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Date: | Tuesday 19 November 1996 |
Time: | 10:10 LT |
Type: | Cessna 421B GOLDEN EAGLE |
Owner/operator: | Crossings Aviation |
Registration: | N8005Q |
MSN: | 421B-0005 |
Total airframe hrs: | 3406 hours |
Engine model: | Continental GTSIO-520-H |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Olympia - Regional, WA -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Tacoma, WA (KTIW) |
Destination airport: | Ontario, OR (KONO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that during climbout on an IFR flight, he frequently checked the wings for ice accumulation, noting what appeared to be a 'mere' trace of ice. At about 13,000 feet msl, with almost no climb at 125 knots indicated airspeed, the pilot pulled the yoke back a little to climb, and the aircraft began to shudder. The pilot then decided to divert, again checking the wings, seeing what he described as a trace of ice. He said he cycled the deice boots with no apparent change in wing appearance. While on approach, he again cycled the boots between 3000 and 2000 feet msl. The pilot stated that about 20-30 feet above the surface, he started a slight roundout, but when he eased back on the yoke, the airplane shuddered and the nose did not raise. At that point, he was ready to touch down, so he pulled back on the yoke while adding power; however, the airplane landed hard and was damaged. Later, the surface deice system was tested. The boots did not hold pressure due to multiple wing boot holes and a shuttle valve internal leak. Functional tests revealed that the control valves did not direct proper pressure to the system, and that the shuttle valves did not direct pressure properly to the boots (there was leakage to the vacuum side of the valves).
Probable Cause: inoperative deicing equipment, due to multiple wing boot holes and malfunctioning control/shuttle valves; subsequent build-up of airframe (wing) ice; and failure of the pilot to maintain adequate airspeed during the flare for landing. Factors relating to the accident included: the adverse weather (icing) conditions, and inadequate maintenance concerning the deicing equipment.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA97LA030 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB SEA97LA030
Location
Revision history:
Date/time | Contributor | Updates |
26-Apr-2023 06:31 |
IJC64 |
Added |
08-Apr-2024 18:00 |
ASN Update Bot |
Updated [Time, Cn, Operator, Total occupants, Other fatalities, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report] |
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