ASN Wikibase Occurrence # 31172
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Date: | Saturday 20 July 1996 |
Time: | 08:57 LT |
Type: | Mitsubishi MU-2B-36 |
Owner/operator: | D & D Aviation |
Registration: | N999FA |
MSN: | 676 |
Year of manufacture: | 1975 |
Total airframe hrs: | 8878 hours |
Engine model: | Garrett TPE-331 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | 2 miles from Scottsdale Municipal Airport, Scottsdale, Arizona -
United States of America
|
Phase: | Initial climb |
Nature: | Executive |
Departure airport: | (KSDL) |
Destination airport: | Phoenix, AZ (KPHX) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The right engine lost power after an uncontained engine failure during the initial takeoff climb. The airplane would not climb and the pilot was forced to land. The pilot selected a street for a forced landing area. The pilot landed gear up while maneuvering to avoid hitting street light poles and automobiles. After touchdown, the airplane slid into a block wall. A fire erupted as a result of a postimpact fuel leak in the left wing. The airplane's engines were examined at the manufacturer's facilities. The right engine exhibited evidence of an uncontained separation of the second stage turbine rotor disk. Examination of the disk fragments revealed a low cycle fatigue fracture mode. The fatigue initiated from multiple areas at and adjacent to the inside diameter bore surface near the aft side of the disk. According to the engine manufacturer, the multiple indication areas were associated with uninspectable size porosity and the primary carbides in the cast material. There were no material or casting defects detected on any of the fractures through the wheel.
Probable Cause: an uncontained failure of the second stage turbine wheel due to fatigue. Factors were: obstructions in the forced landing area and the inability of the airplane to climb after the turbine wheel failure.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX96LA280 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB LAX96LA280
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=999FA Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
01-Aug-2009 07:47 |
harro |
Updated |
01-Aug-2009 07:47 |
harro |
Updated |
10-Sep-2013 06:34 |
wf |
Updated [Operator, Location, Departure airport, Destination airport, Source, Narrative] |
06-Mar-2016 22:52 |
Dr.John Smith |
Updated [Location, Nature, Departure airport, Destination airport, Source, Narrative] |
06-Mar-2016 22:55 |
Dr.John Smith |
Updated [Time, Narrative] |
09-Apr-2024 05:34 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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