Accident Meyers 200A N489C,
ASN logo
ASN Wikibase Occurrence # 311918
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Wednesday 26 May 2021
Time:17:55 LT
Type:Silhouette image of generic M200 model; specific model in this crash may look slightly different    
Meyers 200A
Owner/operator:
Registration: N489C
MSN: 254
Year of manufacture:1959
Total airframe hrs:3601 hours
Engine model:Continental IO-520A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Marathon, Florida -   United States of America
Phase: Landing
Nature:Private
Departure airport:Summerland Key, FL
Destination airport:Marathon, FL
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, during final approach the nose and left main landing gear lights were illuminated green. The red 'in-transit” light was illuminated for the right main landing gear. He overflew the runway and airport personnel confirmed that the right main landing gear was partially extended. He unsuccessfully attempted to cycle, manually extend, and use g-force maneuvers to extend the right main landing gear. The pilot performed a landing and kept the right wing off the ground as long as he could during the landing since the right main landing gear was partially extended. During the landing rollout, the right wing impacted the runway, the airplane veered to the right and came to rest off the right side of the runway, resulting in substantial damage to the right aileron. A post-accident examination of the right main landing gear revealed that the oleo strut was under inflated, therefore, the strut did not extend the wheel properly and could not retract correctly into the right main landing gear wheel well. Then, when the landing gear was extended, the wheel became lodged on the wheel well and could not extend properly. After the airplane was lifted off the runway, the right main landing gear was extended by hand and it locked into place. The most recent annual inspection was performed about 5 months before the accident, and at that time the left main landing gear actuator was serviced. The maintenance entry did not record any service to the right main landing gear.

Probable Cause: The failure of the right main landing gear to fully extend during landing as a result of the underinflated right main landing gear oleo strut.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA21LA235
Status: Investigation completed
Duration: 3 months
Download report: Final report

Sources:

NTSB ERA21LA235

History of this aircraft

Other occurrences involving this aircraft
16 June 2022 N489C Private 0 Weslaco, TX sub

Location

Revision history:

Date/timeContributorUpdates
03-May-2023 05:33 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org