ASN Wikibase Occurrence # 311918
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Date: | Wednesday 26 May 2021 |
Time: | 17:55 LT |
Type: | Meyers 200A |
Owner/operator: | |
Registration: | N489C |
MSN: | 254 |
Year of manufacture: | 1959 |
Total airframe hrs: | 3601 hours |
Engine model: | Continental IO-520A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Marathon, Florida -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Summerland Key, FL |
Destination airport: | Marathon, FL |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, during final approach the nose and left main landing gear lights were illuminated green. The red 'in-transitâ light was illuminated for the right main landing gear. He overflew the runway and airport personnel confirmed that the right main landing gear was partially extended. He unsuccessfully attempted to cycle, manually extend, and use g-force maneuvers to extend the right main landing gear. The pilot performed a landing and kept the right wing off the ground as long as he could during the landing since the right main landing gear was partially extended. During the landing rollout, the right wing impacted the runway, the airplane veered to the right and came to rest off the right side of the runway, resulting in substantial damage to the right aileron. A post-accident examination of the right main landing gear revealed that the oleo strut was under inflated, therefore, the strut did not extend the wheel properly and could not retract correctly into the right main landing gear wheel well. Then, when the landing gear was extended, the wheel became lodged on the wheel well and could not extend properly. After the airplane was lifted off the runway, the right main landing gear was extended by hand and it locked into place. The most recent annual inspection was performed about 5 months before the accident, and at that time the left main landing gear actuator was serviced. The maintenance entry did not record any service to the right main landing gear.
Probable Cause: The failure of the right main landing gear to fully extend during landing as a result of the underinflated right main landing gear oleo strut.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA21LA235 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB ERA21LA235
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
03-May-2023 05:33 |
ASN Update Bot |
Added |
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