ASN Wikibase Occurrence # 313982
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Date: | Monday 28 June 2021 |
Time: | 10:30 |
Type: | Cub Crafters CC11 Carbon Cub |
Owner/operator: | Flight Management LLC |
Registration: | N10TA |
MSN: | CCX-2000-0080 |
Year of manufacture: | 2019 |
Total airframe hrs: | 127 hours |
Engine model: | Lycoming CC363I |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Hood River, OR -
United States of America
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Phase: | Initial climb |
Nature: | Private |
Departure airport: | Ken Jernstedt Airfield, OR (4S2) |
Destination airport: | Ken Jernstedt Airfield, OR (4S2) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On June 28, 2021, about 1030 Pacific daylight time, an experimental amateur-built, CCX-2000 airplane, N10TA, was substantially damaged when it was involved in an accident near Hood River, Oregon. The pilot was not injured. The airplane was operated as a Title 14, Code of Federal Regulations Part 91 personal flight.
The experimental, amateur-built airplane was retrofitted with an experimental exhaust system that comprised a titanium exhaust header and aluminum muffler.
On the first flight with the new exhaust system, the engine lost total power just after takeoff. The pilot performed a forced landing during which the airplane impacted trees, resulting in substantial damage.
Examination of the engine revealed that the muffler inner tube failed due to creep fatigue and fractured into several fragments. Components of the muffler included a perforated inner tube, surrounded by fiberglass packing material held in place by five clamps; an outer shell; end caps; and an inlet and exhaust tube, all constructed out of 6061-T6, an aluminum alloy not suited for use above 350°F to 400°F. Any use near or above that temperature will cause additional heat treatment and changes to the properties and performance of the material. The observation of the creep separation indicates that the material was exposed to much higher temperatures than this, likely between 600°F and 1000°F. It is likely that, when exposed to the hot exhaust gasses during takeoff, the fragments, clamps, and fiberglass packing material migrated aft and collapsed the remaining section of the inner tube, which plugged the exhaust port and resulted in a total loss of power. A postaccident test run of the engine without the muffler revealed no anomalies.
Probable Cause: The total loss of engine power due to improper construction of the muffler, which resulted in separation of the internal components.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | WPR21LA250 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
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Sources:
NTSB
Location
Images:
Revision history:
Date/time | Contributor | Updates |
29-May-2023 20:02 |
Captain Adam |
Added |
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