ASN Wikibase Occurrence # 314324
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Date: | Friday 1 March 2013 |
Time: | 05:00 LT |
Type: | Boeing 737-377 |
Owner/operator: | Jet2 |
Registration: | G-CELS |
MSN: | 23660/1294 |
Year of manufacture: | 1986 |
Engine model: | CFM56-3B2 |
Fatalities: | Fatalities: 0 / Occupants: 6 |
Aircraft damage: | None |
Category: | Incident |
Location: | London, -
United Kingdom
|
Phase: | Standing |
Nature: | Ferry/positioning |
Departure airport: | London-Gatwick Airport (LGW/EGKK) |
Destination airport: | |
Investigating agency: | AAIB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During pre-flight preparations smoke was seen coming from the overhead bin over seat row 1 D, E, F.
The smoke was caused by arcing across the pins of the redundant No 2 Galley electrical connector. Tests
confirmed that the connector remained powered despite the No 2 Galley CB being pulled and collared.
A previous inspection had identified this issue, but the operator’s maintenance systems allowed the task to be closed prior to completion of the rectification work.
The operator has changed the systems used to control such inspections to ensure that additional work must be completed before the inspection is closed. Any aircraft which may have been similarly affected, have been reinspected.
Accident investigation:
|
| |
Investigating agency: | AAIB |
Report number: | EW/C2013/03/01 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB DCA13WA113
Revision history:
Date/time | Contributor | Updates |
02-Jun-2023 16:20 |
ASN Update Bot |
Added |
05-Jun-2023 12:41 |
harro |
Updated |
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