ASN Wikibase Occurrence # 314378
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Date: | Wednesday 15 August 2012 |
Time: | 07:35 LT |
Type: | Cessna 560XL |
Owner/operator: | Elliott Aviation Flight Services Inc |
Registration: | N108EK |
MSN: | 560-5032 |
Total airframe hrs: | 4510 hours |
Engine model: | P&W Canada PW545A |
Fatalities: | Fatalities: 0 / Occupants: 8 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Des Moines, Iowa -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Minneapolis-Flying Cloud Airport, MN (FCM/KFCM) |
Destination airport: | Arlington Municipal Airport, TX (KGKY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight crewmembers reported that, after about 10 minutes of cruise flight at 40,000 ft pressure altitude, they observed an autopilot pitch trim mistrim annunciation and an associated master caution indication. As they began to reference the applicable checklist, the autopilot automatically disengaged, the airplane suddenly pitched down, and the airspeed increased to about 30 knots over the redline. The flight crew regained control of the airplane and then leveled it at 33,000 ft pressure altitude. The flight crew subsequently landed the airplane without further incident. The autopilot was not used after the temporary loss of airplane control; however, the electric pitch trim was used after passing through 10,000 ft mean sea level, and it functioned normally. A postincident examination of the autopilot, pitch trim systems, and horizontal stabilizer did not reveal any anomalies consistent with a loss of control.
Probable Cause: A temporary loss of control during cruise flight for reasons that could not be determined because postincident examination of the autopilot, pitch trim systems, and horizontal stabilizer revealed no anomalies consistent with a loss of control.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN12IA554 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB CEN12IA554
Location
Revision history:
Date/time | Contributor | Updates |
02-Jun-2023 16:46 |
ASN Update Bot |
Added |
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