ASN Wikibase Occurrence # 314388
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 26 July 2012 |
Time: | 15:30 LT |
Type: | American Champion 8KCAB |
Owner/operator: | Private |
Registration: | N60GK |
MSN: | 1115-2012 |
Total airframe hrs: | 11 hours |
Engine model: | Lycoming AEIO-360-H1B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Oshkosh, Wisconsin -
United States of America
|
Phase: | Standing |
Nature: | Demo/Airshow/Display |
Departure airport: | Oshkosh-Wittman Field, WI (OSH/KOSH) |
Destination airport: | Oshkosh-Wittman Field, WI (OSH/KOSH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was performing at an air show and entered the aerobatic box with a 45 degree descending roll. At an airspeed of 150 mph, the pilot pulled up into a loop and then initiated a 'snap-on-top-of-a-loopâ maneuver. The pilot's seat then broke, and the pilot and seatback fell backward onto the rear seat and rear control column, temporarily jamming the flight controls. The pilot was then able to recover the airplane to a 'right-side-upâ position with wings level. He flew away from the crowd to assess the situation and subsequently landed without further incident.
An examination revealed that the airplane's seat bottom frame was not equipped with a required reinforcement truss stiffener. The manufacturer reviewed its production work orders and discovered that a batch of 10 seats were produced that were not constructed with the truss stiffener and, therefore, did not conform with the airplane's production type certificate. As a result of this investigation, the manufacturer added steps to the seat production and inspection procedures to ensure proper seat assembly. Additionally, the manufacturer added to the seat welding fixture a locator (a visual cue) for the truss stiffener parts. Further, Service Letter 437 was published indicating that owners should perform a one-time inspection to ensure that the seat bottom frame contains the required reinforcement truss stiffener.
Probable Cause: The failure of the pilot's seat bottom frame due to the manufacturer's improper production, installation, and inspection of that seat bottom, which resulted in a temporary loss of control during an air show performance.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN12IA498 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB CEN12IA498
Location
Revision history:
Date/time | Contributor | Updates |
02-Jun-2023 16:49 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation