ASN Wikibase Occurrence # 314511
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 11 April 2011 |
Time: | 09:15 LT |
Type: | Beechcraft 90B King Air |
Owner/operator: | University Of Oklahoma, Dept Of Aviation |
Registration: | N37OU |
MSN: | LJ-1428 |
Total airframe hrs: | 2789 hours |
Engine model: | P&WC PT-6A-21 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Chickasha, Oklahoma -
United States of America
|
Phase: | Approach |
Nature: | Training |
Departure airport: | Norman-University of Oklahoma Westheimer Airport, OK (KOUN) |
Destination airport: | Norman-University of Oklahoma Westheimer Airport, OK (KOUN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The certified flight instructor (CFI) reported that the airplane was on a downwind leg for landing when a pilot-rated passenger who was sitting in the cabin told him that the right aileron was partially separated from the airplane. The CFI took control of the airplane and landed it uneventfully. The post incident inspection of the airplane revealed that the two inboard aileron hinges were separated from the airframe. The screws (8 screws, 4 upper, 4 lower) which attached the aileron to the aileron hinge points were seated in the aileron skin, but did not screw into the corresponding nut plates on the aileron hinge points. The aileron was not damaged so a mechanic attached the aileron properly to the aileron hinge points and the airplane was returned to service. Maintenance records indicated that the airplane had undergone a phase inspection 10 days prior to the incident. During the phase inspection, the right aileron was removed to repair some light surface corrosion and was reinstalled on the airplane. The incident occurred 5.3 hours after the phase inspection was performed. Eight years prior to the accident, the aircraft manufacturer issued a communique which stated that their technical support department had received reports that during aileron installation, screws missed the nut plates on the aileron hinge points. It stated that this condition can go unnoticed.
Probable Cause: The mechanic's improper installation of the aileron.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN11IA280 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB CEN11IA280
Location
Revision history:
Date/time | Contributor | Updates |
02-Jun-2023 17:57 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation