Serious incident Bell 430 N430CM,
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ASN Wikibase Occurrence # 314605
 
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Date:Wednesday 4 August 2010
Time:05:45 LT
Type:Silhouette image of generic B430 model; specific model in this crash may look slightly different    
Bell 430
Owner/operator:Chevron USA Inc
Registration: N430CM
MSN: 49090
Total airframe hrs:8288 hours
Engine model:Rolls Royce 250-C40B
Fatalities:Fatalities: 0 / Occupants: 8
Aircraft damage: Minor
Category:Serious incident
Location:Venice, Louisiana -   United States of America
Phase: Standing
Nature:Unknown
Departure airport:Venice, LA
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
On August 4, 2010, at 0645 central daylight time, a Bell Helicopter Textron 430 was on the ground at ground idle power conducting the engine start checklist when the collective went to the full up position. There were no injuries among the passengers and crew. Further inspection of the aircraft revealed that the main rotor collective servoactuator piston rod had fractured. No other airframe damage was noted.

The collective servo actuator was examined in the Bell Helicopter Textron's Field Investigations Laboratory. According to Bell Helicopter Textron, the servo actuator piston rod was found to be fractured as a result of stress corrosion cracking.

In response to this incident, Bell Helicopter Textron issued a number of alert service bulletins to perform a one time inspection of the servo actuator piston rod prior to further flight. This service bulletin only applied to servo actuators manufactured by Woodward HRT. Since this same type of servo actuator was also used on other Bell Helicopter Textron helicopters, additional alert service bulletins were issued.

The Federal Aviation Administration (FAA) incorporated these service bulletins' recommended actions (with some minor revisions) in an Emergency Airworthiness Directive. The FAA's emergency AD followed the issuance of an AD by Transport Canada.

Probable Cause: The fracture of the collective servo actuator piston rod resulting from stress corrosion cracking.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ENG10IA045
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB ENG10IA045

Location

Revision history:

Date/timeContributorUpdates
02-Jun-2023 18:55 ASN Update Bot Added

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