ASN Wikibase Occurrence # 315961
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 28 June 2022 |
Time: | 10:30 LT |
Type: | American Champion 8KCAB |
Owner/operator: | Super D Aviation Training Co LLC |
Registration: | N721SD |
MSN: | 722-93 |
Year of manufacture: | 1993 |
Total airframe hrs: | 2318 hours |
Engine model: | Lycoming IO-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Knoxville, Tennessee -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Knoxville, TN |
Destination airport: | Knoxville, TN |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After performing maneuvers in the local area, the pilot receiving instruction and the flight instructor returned to the departure airport and performed two practice landings. During the third landing, the flight instructor heard a 'bangâ noise and the airplane veered left away from the runway centerline. The airplane came to rest in the grass next to the runway and the airplane's fuselage and rudder were substantially damaged.
A Federal Aviation Administration inspector examined the airplane after the accident. The airplane's left main landing gear had collapsed and the inspector found that the left main landing gear through bolt was fractured. The inspector further reported that the airplane's most recent annual inspection had been completed more than 22 months before the accident. Additionally, the airframe manufacturer's maintenance manual required that the through bolt be removed and inspected at every 100 hour/annual inspection and replaced as necessary, in addition to a mandatory replacement every 500 hours. The airplane's maintenance records did not show when the last though bolt change had occurred. Based on this information, it is likely that the landing gear collapsed due to a failure of the left main landing gear through bolt, and that the through bolt had likely not been maintained in accordance with the airframe manufacturer's requirements.
Probable Cause: The inadequate maintenance of the left main landing gear through bolt, which resulted in a left main landing gear collapse and subsequent runway excursion during landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA22LA296 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
NTSB ERA22LA296
Location
Revision history:
Date/time | Contributor | Updates |
26-Jun-2023 07:41 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation