ASN Wikibase Occurrence # 316581
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Date: | Wednesday 24 November 2021 |
Time: | 13:40 LT |
Type: | Beechcraft A36 |
Owner/operator: | |
Registration: | N4370W |
MSN: | E-559 |
Year of manufacture: | 1974 |
Total airframe hrs: | 5334 hours |
Engine model: | Continental IO-520-BA(10) |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tooele, Utah -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Safford Airport, AZ (SAD/KSAD) |
Destination airport: | Tooele, UT |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that he began a descent to pattern altitude at the destination airport. When he reduced the propeller speed to 2,200 rpm, a 'slapping sort of knock began as well as a shimmy in the plane.â The pilot arrested the descent, observed that the oil temperature and oil pressure were normal, and looked outside the airplane to verify that the flight control surfaces had no issues. The pilot then noticed that the airspeed had decreased to 130 miles per hour and that the controls became 'heavy and very mushy.â The pilot initiated a forced landing to a nearby road but abandoned that plan when he observed a vehicle traveling on the road. The pilot advanced the propeller and throttle levers full forward but received no response from the engine, and he noticed that the cylinder head temperature gauge had 'dropped completely to the left.â The pilot maneuvered the airplane to avoid power lines and landed in an open desert area. During the landing, the airplane struck trees, impacted terrain, and came to rest at a nose-low attitude.
Postaccident examination of the airframe and engine revealed no evidence of any pre-existing mechanical malfunction that would have precluded normal operation. Utilizing the reported fuel quantity at the time of departure and fuel burn rate for the reported power setting, it was determined that the pilot had an adequate amount of fuel for the intended flight. As a result, the reason for the total loss of engine power could not be determined.
Probable Cause: The total loss of engine power for reasons that could not be determined based on available evidence.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR22LA064 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB WPR22LA064
Location
Revision history:
Date/time | Contributor | Updates |
07-Jul-2023 19:09 |
ASN Update Bot |
Added |
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