Date: | Monday 2 July 2001 |
Time: | 08:50 |
Type: | Lockheed L-100-30 Hercules |
Owner/operator: | Lynden Air Cargo |
Registration: | N401LC |
MSN: | 4606 |
Year of manufacture: | 1975 |
Total airframe hrs: | 31652 hours |
Engine model: | Allison 501-D22A |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial, repaired |
Category: | Accident |
Location: | Lake Minchumina Airport, AK (MHM) -
United States of America
|
Phase: | Landing |
Nature: | Cargo |
Departure airport: | Anchorage-Ted Stevens International Airport, AK (ANC/PANC) |
Destination airport: | Lake Minchumina Airport, AK (MHM/PAMH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Lockheed Hercules, N401LC, sustained substantial damage during landing at the Lake Minchumina Airport, Alaska. The airplane was being operated as an instrument (IFR) cross-country cargo flight. The crew of the airplane, consisting of the captain, first officer, flight engineer, and a load master, were not injured. Visual meteorological conditions prevailed, and an IFR flight plan was filed. The flight originated at the Anchorage-Ted Stevens International Airport, Alaska, about 08:00.
The director of operations for the operator reported to the NTSB that the Lake Minchumina Airport has a gravel runway that is oriented on a 020/200 degree heading. He added that the captain flew over the airport to inspect the runway conditions, and subsequently elected to use runway 20. He said that the runway is 4,200 feet long, 90 feet wide, and that the gravel runway had a number of frost-heaves that have developed during the past winter. On initial touchdown the airplane "skipped" as the main wheels touched down on the crest of one of the frost-heaves. The airplane became airborne, floated slightly, and then touched down about 750 feet beyond the approach end of the runway. During the second landing flare, the main landing gear wheels touched on the downhill side of a second frost-heave, which allowed the tail of the airplane to contact the gravel runway. The captain characterized the second touchdown as within acceptable limits, but with a slightly nose high attitude. After touchdown, the captain lowered the nose of the airplane, brought the engines into reverse, and completed the landing. After landing rollout, the airplane was taxied to parking. A postflight inspection by the crew discovered a 4 feet by 2 feet puncture on the belly of the airplane, just forward of the main cargo door.
PROBABLE CAUSE: "The flight crew's improper recovery from a bounced landing. Factors associated with the accident were the selection of an unsuitable landing area, and a rough/uneven landing surface."
Accident investigation:
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Investigating agency: | NTSB |
Report number: | ANC01LA081 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
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Sources:
NTSB
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Other occurrences involving this aircraft Location
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