ASN Wikibase Occurrence # 343192
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Date: | Wednesday 2 August 2023 |
Time: | 07:20 LT |
Type: | Air Tractor AT-502 |
Owner/operator: | Airborne Custom Spraying |
Registration: | N45453 |
MSN: | 502-0122 |
Total airframe hrs: | 11012 hours |
Engine model: | Pratt and Whitney PT6-34 AG |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Aslesen Airport (8MN2), Halstad, MN -
United States of America
|
Phase: | Take off |
Nature: | Unknown |
Departure airport: | Halstad, MN (8MN2) |
Destination airport: | Halstad, MN |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that after loading about 100 gallons of jet fuel and about 420 gallons of aerial spray product, he began a takeoff roll on the 2,506 ft asphalt runway. The pilot attempted to rotate the airplane with about 300 ft of runway remaining. Unable to climb out of ground effect, the pilot attempted to jettison the aerial spray product during and after takeoff. The airplane was airborne for about 200 yards before it settled into the soybean field. The airplane sustained substantial damage to the wings, empennage, and fuselage.
During an interview, the pilot stated that he took off with a tailwind with one notch of flaps and remembers over torquing the engine. He reported that he likely rotated too soon, was slow, and never got out of ground effect. The pilot reported, and a postaccident examination corroborated that, there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause: The pilot's attempt to rotate the airplane without sufficient airspeed which resulted in a lack of climb performance and impact with terrain. Contributing to the accident was the pilot's decision to attempt the takeoff with a tailwind.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN23LA346 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB CEN23LA346
Location
Revision history:
Date/time | Contributor | Updates |
03-Aug-2023 13:25 |
Captain Adam |
Added |
09-Aug-2023 18:51 |
Captain Adam |
Updated |
01-Feb-2024 12:50 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Nature, Departure airport, Destination airport, Source, Narrative] |
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