ASN Wikibase Occurrence # 344717
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Date: | Sunday 20 June 2021 |
Time: | 06:00 LT |
Type: | Grumman G-164B Turbo Ag-Cat |
Owner/operator: | Scott Flying Service |
Registration: | N62375 |
MSN: | 806B |
Year of manufacture: | 1988 |
Total airframe hrs: | 14472 hours |
Engine model: | Honeywell TPE331-1-151G |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sedgwick, Arkansas -
United States of America
|
Phase: | En route |
Nature: | Agricultural |
Departure airport: | Fontaine, AR (KPVT) |
Destination airport: | Sedgwick, AR |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting an agricultural flight when the airplane had a sudden total loss of engine power. The pilot stated that the sound of the engine went from normal to silent, with no indication of an engine issue before the loss of engine power. The airplane impacted a levee and nosed over in a flooded rice field during the forced landing. The airplane's empennage, aft fuselage, and engine mounts were substantially damaged during the forced landing.
A postaccident engine examination and disassembly revealed the torque sensor assembly front spur gear was disengaged from the splined shouldered shaft on which it was installed. Additionally, the self-locking nut that secured the front spur gear to the shaft had backed off which allowed the front spur gear to disengage from the shaft.
The examination and testing were unable to determine if the front spur gear self-locking nut was improperly torqued at installation or if it became loose during operation due a loss of retention. However, had the self-locking nut not been seated properly at installation, the disengagement of the front spur gear would likely have occurred well before the accident (2,541.5 hours since the overhauled torque sensor was installed on the engine). Additionally, no anomalies were found with the self-locking nut to suggest why it would have lost retention during operation.
The engine-driven fuel pump and fuel control unit (FCU) are driven through a series of gears in the accessory gearbox, including the front spur gear, and any failure in the gear train that drives the fuel pump and FCU would prevent the fuel pump from delivering fuel to the FCU to sustain engine operation, resulting in an uncommanded engine shutdown.
Probable Cause: The total loss of engine power due to the failure and disengagement of the torque sensor assembly front spur gear from its splined shouldered shaft due to a loose self-locking nut.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN21LA287 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB CEN21LA287
Location
Revision history:
Date/time | Contributor | Updates |
19-Aug-2023 16:32 |
ASN Update Bot |
Added |
19-Aug-2023 16:37 |
harro |
Updated |
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