Accident Cub Crafters CC11-160 Carbon Cub N825ME,
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ASN Wikibase Occurrence # 345552
 
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Date:Friday 6 August 2021
Time:16:20 LT
Type:Silhouette image of generic PA11 model; specific model in this crash may look slightly different    
Cub Crafters CC11-160 Carbon Cub
Owner/operator:Plane Company LLC
Registration: N825ME
MSN: CC11-00372
Year of manufacture:2015
Total airframe hrs:267 hours
Engine model:Titan OX-340CC-B3J3N4/D3B004
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Springfield, Tennessee -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Springfield, TN
Destination airport:Springfield, TN
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that the engine suddenly stopped producing power while climbing at an altitude of about 400 ft above ground level after a touch-and-go landing. With no time to troubleshoot the reason for the loss of power, the pilot performed a forced landing to a field, where the airplane contacted a fence and the fuselage and right wing were substantially damaged.
Weather conditions in the area at the time of the accident flight were conducive to serious carburetor icing at glide power; however, the description of the partial loss of engine power and the phase of flight at which it occurred were not consistent with carburetor icing.
A postaccident examination and test run revealed that the engine was able to operate normally. During the examination it was noted that a fuel valve was leaking, though it is likely that this was due to damage sustained during the accident. Additionally, the electronic ignition system backup battery voltage was low. During the engine test run when the main ignition system circuit breakers were deactivated, and with the right side backup ignition selected, the engine lost power (and appropriate annunciations were illuminated on the instrument panel). Given that the pilot did not report any ignition system issues or annunciations, it is unlikely that the voltage issue noted with the backup system played a role in the reported loss of engine power. Based on this information, a reason for the loss of engine power could not be determined.

Probable Cause: A loss of engine power for undetermined reasons.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA21LA321
Status: Investigation completed
Duration: 2 years
Download report: Final report

Sources:

NTSB ERA21LA321

Location

Revision history:

Date/timeContributorUpdates
14-Sep-2023 19:29 ASN Update Bot Added
14-Sep-2023 19:33 harro Updated

Corrections or additions? ... Edit this accident description

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