ASN Wikibase Occurrence # 347994
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Date: | Saturday 4 November 2023 |
Time: | 15:00 LT |
Type: | Denney Kitfox 5 |
Owner/operator: | Private |
Registration: | N88VJ |
MSN: | 001 |
Total airframe hrs: | 938 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ririe, ID -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Rigby, ID (U56) |
Destination airport: | Ririe, ID |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot of the tailwheel-equipped airplane intended to spend the day practicing takeoffs and landings at multiple remote backcountry sites with a group of three other similar airplanes. He practiced at the original departure airport before the other group arrived and reported that those flights were nominal. The group then departed for the first intended destination, which was a flat landing site surrounded by tall grass and brush. Those landings were uneventful, so the group decided to proceed to another close landing spot.
This landing area appeared wider and flatter than the previous, however the grass was taller and thicker, such that the ground was obscured. The first airplane landed uneventfully, and the accident pilot decided that rather than landing he would perform a touch-and-go, with the wheels touching the grass so he could assess the conditions. As the pilot began to flare the airplane, he decided that it was safe to proceed with a full-stop landing. As the wheels touched the ground, it became apparent that the surface was much rougher than he anticipated, and the airplane bounced after the main wheels touched two large rocks 200 ft into the ground roll. The pilot retracted the flaperons and as the airplane decelerated the nose began to drop, even though he was holding the control stick full aft. The pilot stated that he was likely inadvertently applying brake pressure as he pushed against the rudder pedals to pull back further on the control stick, and that this may have exacerbated the pitch down motion. The airplane then nosed over.
The airplane came to rest inverted and sustained substantial damage to both wing struts and multiple wing ribs.
Probable Cause: The pilot's inadvertent excessive use of brakes which resulted in a nose-over.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR24LA027 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB WPR24LA027
Location
Revision history:
Date/time | Contributor | Updates |
16-Nov-2023 10:09 |
Captain Adam |
Added |
29-Dec-2023 19:51 |
Captain Adam |
Updated [Time, Departure airport, Category, Accident report] |
11-Feb-2024 11:26 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Source, Narrative] |
11-Feb-2024 11:49 |
ASN |
Updated [Operator, Narrative] |
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