ASN Wikibase Occurrence # 34871
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Date: | Tuesday 23 December 1997 |
Time: | 19:14 LT |
Type: | Piper PA-28-181 |
Owner/operator: | Jose Mitja |
Registration: | N8074Z |
MSN: | 28-8090063 |
Total airframe hrs: | 2575 hours |
Engine model: | Lycoming O-360-A4M |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Tallahassee, FL -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Columbus, GA (KCSG) |
Destination airport: | (KTLH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was executing the ILS runway 36 approach when the airplane struck a 150 foot high power line, located about 2.5 miles south of the airport. The local air traffic controller stated that shortly after clearing the accident airplane to land, the tower had a power interruption which caused the radar to blink and get skewed. She then noticed the airplane's data block disappeared. Prior to the power outage, she had been looking out the window to check the weather conditions, and did not notice any problems with the airplane. The approach controller stated he did not notice anything unusual with the airplane after handing it off to the tower. He stated the airplane's altitude appeared normal, and he did not see it deviate from the localizer. According to the supervisor, he saw a low altitude alert for the airplane, which was followed shortly by the interruption of power to the building. He did not see the airplane make any lateral deviations from the localizer. The reported weather consisted of a 500 feet overcast and 3 miles visibility. Examination of the airplane did not disclose evidence of mechanical malfunction. The minimum altitude for the approach was 376 feet above the ground. A flight test of the ILS navigational facility did not disclose anomalies.
Probable Cause: The pilot's failure to maintain the proper glidepath and adequate obstacle clearance which resulted in collision with a power transmission line.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL98FA030 |
Status: | Investigation completed |
Duration: | 2 years 1 month |
Download report: | Final report |
|
Sources:
NTSB ATL98FA030
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
08-Apr-2024 11:21 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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