ASN Wikibase Occurrence # 349229
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Date: | Tuesday 15 April 1997 |
Time: | |
Type: | Diamond DA20-A1 Katana |
Owner/operator: | Ottawa Aviation Services |
Registration: | C-FTKZ |
MSN: | |
Fatalities: | Fatalities: / Occupants: |
Aircraft damage: | |
Location: | Cornwall Regional Airport, Ontario -
Canada
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | TSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The aircraft, with an instructor pilot and private pilot on board, departed Ottawa, Ontario, on a planned night cross-country training flight to Cornwall,, Mirabel, Quebec, and return to Ottawa. During the climb to cruise flight, the smell of hot oil was detected in the cockpit. The engine oil temperature was observed to be higher than normal, but the oil pressure was normal. The smell was attributed to possible spillage during the addition of oil to the aircraft engine (Bombardier-Rotax GMBH Type 912A3) before departure. The smell faded away and did not reoccur, so the flight was continued. After arriving at Cornwall, a touch-and-go landing was completed on runway 28. At about 300 feet above ground level (agl), the after take-off checks were completed and the engine oil temperature was again noted to be higher than normal, but now the oil pressure was observed to be lower than normal. At about 500 feet agl, a decision was made to return to the airport and land on the reciprocal runway, runway 10. The private pilot completed the turn back to the airport; however, being close to the runway the aircraft was high on the approach. The private pilot placed the aircraft into a forward slip to quickly lose altitude, but the instructor determined that the aircraft could not be landed on the remaining runway without experiencing a runway excursion. The instructor pilot took control of the aircraft and initiated an overshoot at low level. Shortly thereafter the aircraft engine lost all power, and the instructor pilot carried out a forced landing into a field adjacent to the airport. During the landing, the nose gear was torn from the aircraft causing the aircraft to flip over. The crew sustained minor injuries, and the aircraft was substantially damaged.
Accident investigation:
|
| |
Investigating agency: | TSB |
Report number: | A97O0055 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
TSB
Revision history:
Date/time | Contributor | Updates |
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