ASN Wikibase Occurrence # 352173
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 21 May 2022 |
Time: | 13:53 LT |
Type: | Evektor EV-97 SportStar |
Owner/operator: | Ajilix Aerospace LLC |
Registration: | N503RK |
MSN: | 20050503 |
Year of manufacture: | 2006 |
Total airframe hrs: | 539 hours |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lancaster-Fairfield County Airport, OH (KLHQ) -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Lancaster-Fairfield County Airport, OH (KLHQ) |
Destination airport: | Lancaster-Fairfield County Airport, OH (KLHQ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot observed a reduction in engine power shortly after takeoff. While attempting to return to the airport, the engine lost power completely while on the downwind leg of the airport traffic pattern, after which the pilot performed an off-airport landing. The airplane's fuselage and horizontal stabilizer were substantially damaged during the landing.
Postaccident examination of the engine revealed that the pushrod O-rings had been incorrectly installed. This improper installation led to the disintegration of the O-rings, and the resulting debris to blocked the oil ports to the No. 4 connecting rod bearing. The lack of oil to the bearing resulted in the failure of the connecting rod, and the subsequent total loss of engine power.
The airplane's maintenance logbooks did not document any recent engine maintenance that would have required removing the engine's cylinder heads. The cylinders were removed and reinstalled following repair nearly 9 years, and about 58 tachometer hours, before the accident. Based on available information, it is likely that the O-rings were improperly installed during this maintenance.
Probable Cause: The improper installation and subsequent failure of the pushrod O-rings, which resulted in failure of the No. 4 connecting rod due to oil starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA22LA241 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB ERA22LA241
Location
Revision history:
Date/time | Contributor | Updates |
03-Mar-2024 15:23 |
ASN Update Bot |
Added |
03-Mar-2024 15:32 |
ASN |
Updated [Aircraft type, Operator, Location, Departure airport, Destination airport, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation