ASN Wikibase Occurrence # 352255
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Date: | Monday 27 December 1999 |
Time: | 19:00 LT |
Type: | Cessna 172L |
Owner/operator: | Southernaire Carrier, Inc. |
Registration: | N172GT |
MSN: | 17259831 |
Year of manufacture: | 1971 |
Total airframe hrs: | 2139 hours |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | New Orleans-Lakefront Airport, Louisiana (KNEW) -
United States of America
|
Phase: | |
Nature: | Private |
Departure airport: | New Orleans-Lakefront Airport, LA (KNEW) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Cessna 172L airplane, N172GT, was substantially damaged when it collided with a seawall and hangar during engine start at the Lakefront Airport, near New Orleans, Louisiana
When the pilot attempted to start the airplane's engine, the starter's bendix drive gear did not engage the starter ring gear. The pilot stated that he turned off the ignition, took out the key and put it in his pocket, pulled the throttle to the idle position, set the parking brake and got out of the airplane. He chocked the airplane and then slowly rotated the propeller until he felt one piston 'move to top center.' He then got back in the airplane and attempted another start; however, the starter's bendix drive gear still did not engage the starter ring gear. Once again he turned off the ignition, took out the key and put it in his pocket, pulled the throttle to the idle position, and got out of the airplane. As he manually rotated the propeller, the engine started.
The airplane jumped the chocks, began traveling forward unoccupied and impacted a sea wall and hangar. The pilot stated that he thought that the mixture was off. During an examination of the starter system, an intermittent short was found in the starter switch, which allowed the magnetos to remain ungrounded or 'hot' with the switch in the 'off' position.
Probable Cause: The pilot's inadvertent starting of the engine. Factors were the pilot's failure to set the mixture control to the off position, and the intermittent short in the starter switch.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW00LA055 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB FTW00LA055
Location
Revision history:
Date/time | Contributor | Updates |
06-Mar-2024 15:31 |
ASN Update Bot |
Added |
06-Mar-2024 16:45 |
ASN |
Updated [Location, Departure airport, Destination airport, Narrative] |
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