ASN Wikibase Occurrence # 352264
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 25 December 1999 |
Time: | 15:00 LT |
Type: | Van's RV-4 |
Owner/operator: | Private |
Registration: | N8ZZ |
MSN: | 3407 |
Total airframe hrs: | 230 hours |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Florence, New Jersey -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Philadelphia-North Philadelphia Airport, PA (PNE) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:About 30 minutes after takeoff, the pilot felt a 'buzz,' which lasted approximately 2 seconds. The airplane then shook violently, so the pilot retarded the throttle to reduce the shaking. He then turned the magnetos off, one at a time, and reapplied power, but the shaking returned with each power application. Carburetor heat was also applied, with no effect. The pilot then tried to add enough power to maintain altitude, but still found that its application resulted in violent shaking. Power was again reduced to keep the airplane controllable. The pilot attempted to guide the airplane to a nearby airport, but could not hold altitude, and headed for a plowed field. He tried to align the airplane with the furrows, but was unable to due to the approach angle. Upon touchdown, the landing gear collapsed, and the wing spars were damaged. During post-flight examination, part of one of the wooden propeller blades was found to be missing. There was no evidence of a bird strike. The propeller had been bolted onto the hub with the correct torque's, and the cowling had been found securely fastened to the airframe. The engine was also examined, with no significant anomalies noted, and there was no indication of airframe flutter.
Probable Cause: Failure of one of the propeller blades. A factor was the necessity land across, rather than in alignment with, the furrowed terrain due to the nature of the emergency.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC00LA061 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB NYC00LA061
Revision history:
Date/time | Contributor | Updates |
06-Mar-2024 17:38 |
ASN Update Bot |
Added |
06-Mar-2024 17:56 |
ASN |
Updated [Location, Phase, Departure airport, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation