Runway incursion Serious incident Boeing 767-222 N610UA,
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ASN Wikibase Occurrence # 352332
 
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Date:Saturday 20 November 1999
Time:22:07 LT
Type:Silhouette image of generic B762 model; specific model in this crash may look slightly different    
Boeing 767-222
Owner/operator:United Airlines
Registration: N610UA
MSN: 21871/15
Year of manufacture:1982
Engine model:P&W JT9D-7R4D
Fatalities:Fatalities: 0 / Occupants: 179
Aircraft damage: None
Category:Serious incident
Location:New York-John F. Kennedy International Airport, NY (JFK/KJFK) -   United States of America
Phase: Approach
Nature:Passenger - Scheduled
Departure airport:San Francisco International Airport, CA (SFO/KSFO)
Destination airport:New York-John F. Kennedy International Airport, NY (JFK/KJFK)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While on final, the first officer had trouble trimming the airplane. The captain attempted to trim the airplane via his yoke switch and the manual trim handle, with no success. A go-around was executed. The crew ran the checklist, but control of the stabilizer trim was not regained. The crew pulled circuit breakers H11 and H20, and then reset them. The stabilizer trim was still inoperative. The crew reset the trim cutout switches twice, and normal operation of the stabilizer trim was reestablished. The left stabilizer position transmitter, and the right stabilizer position transmitter were out of calibration. Also, the left stabilizer trim control module (STCM) was found to have a higher than normal leakage, and the connector for the corresponding shut-off valve was shorting across several of its pins due to skydrol incursion. No faults were identified for the right system except for the right-stabilizer-position transmitter. According to the operator, the system should have operated at half rate with the above discrepancy, but did not. There have been no reports of difficulties with the airplane's stabilizer trim system since the event.

Probable Cause: Total failure of the stabilizer control system for undetermined reasons.

Accident investigation:
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Investigating agency: NTSB
Report number: NYC00IA036
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB NYC00IA036

Location

Revision history:

Date/timeContributorUpdates
07-Mar-2024 10:57 ASN Update Bot Added
07-Mar-2024 10:59 ASN Updated [Aircraft type, Location, Nature, Departure airport, Destination airport, Narrative]

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