Accident American General AG-5B Tiger N1195L,
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ASN Wikibase Occurrence # 352350
 
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Date:Friday 12 November 1999
Time:18:38 LT
Type:Silhouette image of generic AA5 model; specific model in this crash may look slightly different    
American General AG-5B Tiger
Owner/operator:Private
Registration: N1195L
MSN: 10095
Year of manufacture:1992
Total airframe hrs:1022 hours
Engine model:Lycoming O-360-A4K
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Van Nuys, CA -   United States of America
Phase: Approach
Nature:Unknown
Departure airport:(KVNY)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The outboard 1/3 of the aircraft's left wing was deformed upward about 5 degrees with respect to the inboard section during an encounter with wake turbulence while on downwind leg for landing. The upper wing skins of both wings exhibited compression buckling, and the mass balance weights on both ailerons were separated and fell from the aircraft. The pilot reported that the flight was unremarkable until, while downwind for landing, there was an instantaneous jolt of sudden severe turbulence that ended before he could take any action. Data obtained from the airport noise abatement office showed that 2 minutes 23 seconds prior to the encounter, a heavy transport aircraft passed over the location on an ILS approach to another airport 6 miles away; the transport airplane was about 500 feet higher than the accident airplane as it crossed the location. The air traffic control tower at the airport where the accident occurred made a wake turbulence cautionary broadcast to all aircraft 30 seconds prior to when the accident aircraft first contacted the tower for landing. The cautionary broadcast was not repeated.

Probable Cause: The pilot's encounter with unknown and unanticipated wake turbulence from a heavy transport aircraft, which was landing at another airport. A factor in the accident was the tower controller's failure to repeat a previously broadcast wake turbulence cautionary advisory when the aircraft later checked in on tower frequency.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX00LA035
Status: Investigation completed
Duration: 1 year and 9 months
Download report: Final report

Sources:

NTSB LAX00LA035

Location

Revision history:

Date/timeContributorUpdates
07-Mar-2024 11:17 ASN Update Bot Added

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