Airprox Accident McDonnell Douglas DC-10-30F N602GC,
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Date:Sunday 7 November 1999
Time:22:20 LT
Type:Silhouette image of generic DC10 model; specific model in this crash may look slightly different    
McDonnell Douglas DC-10-30F
Owner/operator:Gemini Air Cargo
Registration: N602GC
MSN: 47923/196
Total airframe hrs:98292 hours
Engine model:General Electric CF6-5002
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: Substantial
Category:Accident
Location:near Honolulu, HI -   United States of America
Phase: En route
Nature:Cargo
Departure airport:Honolulu Airport, HI (HNL)
Destination airport:Nadi International Airport (NAN/NFFN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The DC-10 captain, in response to a Traffic Collision Avoidance System (TCAS) alert, made an aggressive pitch change and felt a slight buffet as the airplane decelerated. The maneuver resulted in wrinkling of the elevator skins. Air Traffic Control (ATC) instructed a DC-9 crew to maintain visual separation and the DC-9 crew accepted the instruction. The airplanes were about 7 miles from each other in night conditions on converging courses; the DC-9 was descending out of 5,000 feet and the DC-10 was climbing through 3,800 feet. The controller had to repeat instructions to the DC-10 crew, as well as other crews. One crew informed ATC that their radio transmissions were weak.
Douglas Flight Operation Letter AOL, C1-E60-HHK-L033 dated January 21, 1988, explained probable resultant damage to aircraft components when speed was reduced to buffet speeds indicated on the Cruise Buffet Onset Boundary Chart as presented in the DC-10 Aircraft Flight Manual. It noted that in some cases this buffeting resulted in wrinkled outboard elevator skins. It emphasized that speed reduction down to or near the clean configuration stalling speed greatly increased the chance of experiencing elevator damage.

Probable Cause: The pilot-in-command initiated an evasive manuver during a near midair collission. The airplane entered a prestall buffet, which resulted in buckling of the elevator skins.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX00FA041
Status: Investigation completed
Duration: 2 years and 8 months
Download report: Final report

Sources:

NTSB LAX00FA041

Revision history:

Date/timeContributorUpdates
08-Mar-2024 08:18 ASN Update Bot Added
08-Mar-2024 08:22 ASN Updated [Aircraft type, Cn, Location, Nature, Departure airport, Destination airport, Narrative]

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