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Date: | Sunday 7 November 1999 |
Time: | 22:20 LT |
Type: | McDonnell Douglas DC-10-30F |
Owner/operator: | Gemini Air Cargo |
Registration: | N602GC |
MSN: | 47923/196 |
Total airframe hrs: | 98292 hours |
Engine model: | General Electric CF6-5002 |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Honolulu, HI -
United States of America
|
Phase: | En route |
Nature: | Cargo |
Departure airport: | Honolulu Airport, HI (HNL) |
Destination airport: | Nadi International Airport (NAN/NFFN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The DC-10 captain, in response to a Traffic Collision Avoidance System (TCAS) alert, made an aggressive pitch change and felt a slight buffet as the airplane decelerated. The maneuver resulted in wrinkling of the elevator skins. Air Traffic Control (ATC) instructed a DC-9 crew to maintain visual separation and the DC-9 crew accepted the instruction. The airplanes were about 7 miles from each other in night conditions on converging courses; the DC-9 was descending out of 5,000 feet and the DC-10 was climbing through 3,800 feet. The controller had to repeat instructions to the DC-10 crew, as well as other crews. One crew informed ATC that their radio transmissions were weak.
Douglas Flight Operation Letter AOL, C1-E60-HHK-L033 dated January 21, 1988, explained probable resultant damage to aircraft components when speed was reduced to buffet speeds indicated on the Cruise Buffet Onset Boundary Chart as presented in the DC-10 Aircraft Flight Manual. It noted that in some cases this buffeting resulted in wrinkled outboard elevator skins. It emphasized that speed reduction down to or near the clean configuration stalling speed greatly increased the chance of experiencing elevator damage.
Probable Cause: The pilot-in-command initiated an evasive manuver during a near midair collission. The airplane entered a prestall buffet, which resulted in buckling of the elevator skins.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX00FA041 |
Status: | Investigation completed |
Duration: | 2 years and 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX00FA041
Revision history:
Date/time | Contributor | Updates |
08-Mar-2024 08:18 |
ASN Update Bot |
Added |
08-Mar-2024 08:22 |
ASN |
Updated [Aircraft type, Cn, Location, Nature, Departure airport, Destination airport, Narrative] |
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