ASN Wikibase Occurrence # 352589
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Date: | Saturday 25 September 1999 |
Time: | 11:30 LT |
Type: | Glasair II |
Owner/operator: | Private |
Registration: | N55BP |
MSN: | 2281 |
Total airframe hrs: | 550 hours |
Engine model: | Lycoming IO-360 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | River Ranch, FL -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Lakeland, FL (KLAL) |
Destination airport: | (2RR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Upon arrival at his destination airport, the pilot entered the traffic pattern for landing. When engine power was reduced, the engine started to sputter. The pilot increased power, turned the boost pump on, and changed the fuel selector valve with negative results. He informed UNICOM that he would be unable to make the runway. A local highway was obstructed due to vehicle traffic and a forced landing was conducted to a marshy area. Examination of the engine assembly and accessories did not reveal the cause of engine roughness or subsequent total loss of engine power.
Probable Cause: A total loss of engine power for undetermined reasons, which resulted in a forced landing to non-suitable terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA99LA268 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB MIA99LA268
Location
Revision history:
Date/time | Contributor | Updates |
08-Mar-2024 08:29 |
ASN Update Bot |
Added |
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