Accident Cessna 172RG N6231V,
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ASN Wikibase Occurrence # 352765
 
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Date:Saturday 21 August 1999
Time:10:59 LT
Type:Silhouette image of generic C172 model; specific model in this crash may look slightly different    
Cessna 172RG
Owner/operator:Golden Express Aviation
Registration: N6231V
MSN: 172RG0594
Total airframe hrs:4950 hours
Engine model:Lycoming O-360-F1A6
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Miami, FL -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:(KTMB)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that after takeoff while climbing through 500 feet, the airplane abruptly and uncommanded, yawed to the left. He attempted to correct with rudder trim but the trim wheel turned freely. The flight remained in the traffic pattern and while on short final approach, the controller advised the pilot to go-around as the landing gear was not extended. The pilot lowered the landing gear but landed before the main landing gear locked in place. He stated that he heard the gear warning horn while on short final approach with the flaps extended. Post accident examination of the airplane revealed that a wire at the micro-switch for the throttle gear warning was broken; the wire was reconnected and the warning horn operated normally. The rudder trim actuator and trim wheel were fully displaced to the left, and the master link for the rudder trim chain was noted to be bent and the master link lock clip was fractured. Metallurgical examination of the lock clip revealed it failed due to overstress failure. Post accident retraction and extension tests of the landing gear revealed no evidence of preimpact failure or malfunction.

Probable Cause: The delay by the pilot-in-command to extend the gear resulting in collapse of the main landing gear after touchdown. Factors in the accident were the inoperative gear warning system associated with the throttle due to the broken wire at the throttle microswitch, and the overstress failure of the rudder trim chain master link clip which resulted in disconnection of the rudder trim while trimmed full left.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA99LA233
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB MIA99LA233

Location

Revision history:

Date/timeContributorUpdates
08-Mar-2024 17:51 ASN Update Bot Added

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