Accident Beechcraft B55 Baron N210WW,
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ASN Wikibase Occurrence # 35277
 
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Date:Wednesday 20 November 1996
Time:12:08 LT
Type:Silhouette image of generic BE55 model; specific model in this crash may look slightly different    
Beechcraft B55 Baron
Owner/operator:Monib Ali Hohandiss
Registration: N210WW
MSN: TC-1774
Total airframe hrs:2570 hours
Engine model:Continental IO-470-L
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Goleta, CA -   United States of America
Phase: Approach
Nature:Private
Departure airport:Long Beach, CA (KLGB)
Destination airport:Santa Barbara, CA
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During IFR arrival, the pilot was cleared for an ILS runway 7 approach after being vectored to intercept the localizer from the south side. Last assigned altitude was 2000' msl. Radar data showed the aircraft (acft) continued across the localizer toward rising terrain. Air traffic controllers (ATC) issued instructions to turn back to the localizer, but the pilot did not follow. ATC then issued urgent instructions to turn & climb. (Later, they said he calmly acknowledged their transmissions, but continued toward rising terrain.) Radar contact was lost, but the airplane finally turned south. However, it hit avacado trees on the west side of sloping terrain at about 440' msl, while in a steep bank. No preimpact mechanical anomaly was found that would have resulted in the accident. The pilot's former wife recalled instances when he had miss-set the autopilot OBS; on those occasions, he had similarly deviated from the localizer at intercept & resisted her suggestion to take over manually & fly the approach, but persisted in trying to make the autopilot fly the approach. A flight instructor, who administered a biennial flight review 1 month earlier, found the pilot's instrument flight skills weak & refused to certify his instrument competency. Toxicology tests of tissue from the pilot indicated the presence of a narcotic pain reliever and its metabolite. Tests of kidney tissue showed 0.337 mcg/ml Propoxyphene & 2.7 mcg/ml Norpropoxyphene; tests of muscle tissue showed 0.385 mcg/ml Propoxyphene and 1.9 mcg/ml Norpropoxyphene.

Probable Cause: failure of the pilot to maintain control of the aircraft during an instrument approach, due to spatial disorientation, and/or his failure to maintain proper altitude. Factors relating to the accident were: the pilot's delay (or failure) to initiate a missed approach, and his lack of instrument competency.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX97FA046
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB LAX97FA046

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
08-Jun-2023 04:02 Ron Averes Updated
08-Apr-2024 17:55 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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