ASN Wikibase Occurrence # 352949
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 24 July 1999 |
Time: | 13:30 LT |
Type: | Beechcraft C23 |
Owner/operator: | Private |
Registration: | N63TW |
MSN: | M-1762 |
Total airframe hrs: | 1764 hours |
Engine model: | Lycoming O-360-A4J |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Seneca, SC -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | (KCEU) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After flying in the local area for about 30 minutes, the flight returned to the departure airport, and landed. The airplane impacted the runway, bounced twice, skidded off the left side of the runway, hit a ditch and embankment. The pilot attempted to make the takeoff with full flaps, but immediately retracted all the flaps when the aircraft would not climb.
Probable Cause: the pilot misjudged the flare, landed hard, bounced, departed the runway, which resulted in an impact with a ditch and embankment. A factor in this accident was the improper recovery from a bounced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA99LA202 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB MIA99LA202
Location
Revision history:
Date/time | Contributor | Updates |
09-Mar-2024 08:34 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation