Accident Velocity XL/RG N19DW,
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ASN Wikibase Occurrence # 353173
 
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Date:Tuesday 15 June 1999
Time:10:04 LT
Type:Silhouette image of generic VELO model; specific model in this crash may look slightly different    
Velocity XL/RG
Owner/operator:Private
Registration: N19DW
MSN: 3RX026
Total airframe hrs:117 hours
Engine model:Lycoming IO-540-E4C5
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Fort Pierce, FL -   United States of America
Phase: En route
Nature:Private
Departure airport:Hollywood, FL (HWO
Destination airport:Fort Pierce, FL
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While maneuvering in cruise flight, the pilot/builder of the experimental airplane noticed a fluctuating fuel pressure gage and then the engine quit. The pilot executed a forced landing onto an interstate highway. Postcrash examination revealed an empty right wing fuel tank and no other abnormality of the fuel system and engine. Postcrash start and operation of the engine was satisfactory. The pilot/builder revealed that ever since he changed fuel filler caps, two flights before the accident flight, he had experienced fuel tank imbalance problems. A factory test pilot, using wing tank caps of various tightness adjustments, revealed that gravity feed from wing tank to sump tank could be interrupted if the cap were allowed to fit loosely and allow siphoning due to upper wing surface low pressure while inflight. As a result of the testing, the factory has increased the size of the fuel vent plumbing, eliminated the sump tank vent in favor of an air bleed, 'burp valve', and sent out alerts to all kit owners about fuel starvation resulting from loose-fitting caps.

Probable Cause: The owner/pilot mechanic's failure to adjust the newly installed wing fuel caps resulting in the loss of engine power while in cruise flight due to fuel starvation and the subsequent collision with transmission wires while attempting a forced landing to a highway. Factors in the accident were the failure of the vent system to adequately compensate for the pressure differential created and the failure of the pilot to monitor fuel balance.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA99LA184
Status: Investigation completed
Duration: 1 year and 8 months
Download report: Final report

Sources:

NTSB MIA99LA184

Location

Revision history:

Date/timeContributorUpdates
09-Mar-2024 11:09 ASN Update Bot Added

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