ASN Wikibase Occurrence # 353473
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Date: | Saturday 19 December 1998 |
Time: | 19:14 LT |
Type: | Piper PA-24-250 |
Owner/operator: | Private |
Registration: | N5836P |
MSN: | 24-917 |
Year of manufacture: | 1959 |
Total airframe hrs: | 5110 hours |
Engine model: | Lycoming O-540-A1A5 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Clearwater, FL -
United States of America
|
Phase: | Initial climb |
Nature: | Training |
Departure airport: | (KPIE) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The student had failed the soft field takeoff procedure during a commercial checkride 3 days earlier and was flying with his flight instructor for additional training. The instructor stated that the student had the tendency to allow the airplane to drift to the left after the nose wheel came off the ground. The flight departed and with the student performing a soft field takeoff, the airplane began drifting to the left. The instructor advised the student to apply 'a lot more right rudder!' and the student applied 'way too much' right rudder. While flying in a cross controlled condition, the instructor attempted to regain control but the airplane stalled and the left wing of the airplane contacted the runway, followed by the right wing. The airplane then traveled off the runway onto grass and came to rest with the right main landing gear collapsed. The instructor stated that he should have taken corrective action sooner. Examination of the airplane revealed a bent and broken threaded portion of a rod end for the retract/extension rod.
Probable Cause: The delay by the pilot-in-command (CFI) to take control of the airplane and inadvertent stall/mush resulting in the uncontrolled descent and impact with the runway.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA99LA052 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB MIA99LA052
History of this aircraft
Other occurrences involving this aircraft
19 April 1985 |
N5836P |
William . Rumpf |
0 |
Fellsmere, FL |
|
sub |
23 August 2016 |
N5836P |
Private |
0 |
Nashville International Airport (KBNA), Nashville, TN |
|
min |
Gear-up landing |
Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 07:10 |
ASN Update Bot |
Added |
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