ASN Wikibase Occurrence # 353644
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Date: | Wednesday 21 October 1998 |
Time: | 11:15 LT |
Type: | McDonnell Douglas MD-11F |
Owner/operator: | Federal Express |
Registration: | N581FE |
MSN: | 48419/450 |
Total airframe hrs: | 26857 hours |
Engine model: | GE CF6-80C2D1F |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | None |
Category: | Serious incident |
Location: | Honolulu, HI -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | (KHNL) |
Destination airport: | Sydney Australi, OF |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The first officer was the flying pilot and detected a right wing heavy condition with roll control difficulties during liftoff. The crew dumped fuel and returned for a landing. Post landing inspection showed that three of the five spoilers on top of the right wing were fully deployed. Mechanics found a general-purpose shop rag lodged in the spoiler control pulley system, jamming it in the deployed position. The pulley area where the mechanics found the rag was an open and unprotected area in the center body landing gear wheel well. The center gear doors are normally closed on the ground; however, maintenance personnel can open the doors to work in this area. The doors open and the center landing gear retracts forward into this area during normal operation. The last maintenance completed in this area was 2 days prior to the incident when a contract fuel systems repair company opened several lines in that area to check for leaks. Mechanics could not find any rags, so a supervisor brought rags from another hangar. The supervisor was positive that he provided diaper style rags rather than shop style rags. His company only used the diaper style rag because it was more absorbent than a regular shop rag. A mechanic for the carrier said they normally used colored general-purpose shop towels. They occasionally used white terrycloth towels. The airplane completed 9 flights through various line stations prior to the mishap. On a walk around inspection, mechanics do not normally open the wheel well doors and look at the spoiler pulley system.
Probable Cause: A jammed spoiler control pulley system caused by a shop rag left in an area of recent maintenance. Neither the maintenance organization nor the mechanic responsible could be determined.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX99IA013 |
Status: | Investigation completed |
Duration: | 2 years and 6 months |
Download report: | Final report |
|
Sources:
NTSB LAX99IA013
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 09:00 |
ASN Update Bot |
Added |
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