Accident Cessna 207A N6874M,
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ASN Wikibase Occurrence # 353681
 
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Date:Thursday 8 October 1998
Time:14:15 LT
Type:Silhouette image of generic C207 model; specific model in this crash may look slightly different    
Cessna 207A
Owner/operator:Hageland Aviation Services Inc
Registration: N6874M
MSN: 20700671
Year of manufacture:1980
Total airframe hrs:14681 hours
Engine model:Continental IO-520-F27B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Napaskiak, AK -   United States of America
Phase: Take off
Nature:Unknown
Departure airport:(KPKA)
Destination airport:Bethel, AK (BET)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The certificated airline transport pilot, with one passenger, was departing for another airport about 5 miles away. During the takeoff run, the engine surged. The pilot aborted the takeoff and returned to the departure point of the runway. He said he performed an engine power check which appeared satisfactory, and continued a second takeoff. The pilot did not recheck the fuel system for contamination. Following the second takeoff, the airplane climbed to about 300 feet msl, and the engine RPM suddenly dropped to idle. Emergency procedures did not restore power. The airplane collided with trees during an off-airport landing, and received impact damage to both wing fuel tanks. The airplane came to rest inverted. The pilot said he drained every fuel sump on the airplane at the beginning of the day, and again before beginning the flight to pick up the passenger. Following retrieval of the airplane, an FAA airworthiness inspector examined the airplane. He found about 1/2 cup of water in the fuel system. One wing sump drain was partially blocked by silt. With clean fuel, the engine was started and ran at an idle. The engine later produced full power on an engine test stand.

Probable Cause: The pilot's inadequate preflight inspection to remove all contaminated fuel from the fuel system. Factors in the accident were the pilot's inadequate planning/decision to continue a second takeoff following an engine surge and aborted takeoff, and unsuitable terrain for a forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC99LA002
Status: Investigation completed
Duration: 2 years and 4 months
Download report: Final report

Sources:

NTSB ANC99LA002

Location

Revision history:

Date/timeContributorUpdates
10-Mar-2024 09:25 ASN Update Bot Added

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