ASN Wikibase Occurrence # 353693
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Date: | Saturday 3 October 1998 |
Time: | 10:30 LT |
Type: | Piper PA-28R-200 |
Owner/operator: | Aeronautical Services, Inc. |
Registration: | N53EN |
MSN: | 28R-7335299 |
Year of manufacture: | 1973 |
Total airframe hrs: | 3912 hours |
Engine model: | Lycoming IO-360-C1C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Punta Gorda, FL -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KPGD) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The engine oil was reportedly changed and replenished then the engine was started and operated for about 5-10 minutes. The pilot and General Manager reported verifying that the engine oil quantity was full before the flight departed. During the upwind leg of the second touch-and-go landing, the engine failed. While descending for a forced landing, the airplane collided with trees then the ground. Examination of the airplane by an FAA airworthiness inspector 2 days after the accident revealed no evidence of oil discharge during flight. Disassembly of the engine revealed that the Nos. 2 and 4 connecting rod bearings were failed, and the Nos. 1 and 3 connecting rod bearings were damaged. Minimal oil was found in the engine. No failure or malfunction was noted on the oil pump gears. The hour meter historically indicated a greater elapsed time than the cable driven tachometer during flights of varying lengths; however, during the accident flight, the tachometer elapsed time was greater than the hour meter time. The hour meter is electrically activated by a pressure switch which requires a minimum oil pressure of 3 psi. No malfunction of the hour meter and pressure switch were noted when tested post accident.
Probable Cause: The failure of maintenance personnel to refill the engine oil following the draining of the oil and changing of the oil filter. Also, inadequate preflight of the airplane by the pilot for his failure to noted the absence of engine oil.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | MIA99LA003 |
Status: | Investigation completed |
Duration: | 2 years and 4 months |
Download report: | Final report |
|
Sources:
NTSB MIA99LA003
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 09:32 |
ASN Update Bot |
Added |
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